Laserfiche WebLink
• _ EuuuNv G. BXuwry JX. <br /> >i - wEn"on <br /> ........�to <br /> ENVIRONMENTAL <br /> TAL PROTECTION <br /> Water Boards `"`"°""`""`°"°""'°" <br /> Central Valley Regional Water Quality Control Board <br /> RECEIVED <br /> 20 May 2014 <br /> MAY 21 2014 <br /> Ms. Jennifer Sedlachek <br /> Exxon/Mobil Environmental Services Company ENVIRONMENTAL HEALTH <br /> 4096 Piedmont Ave, #194 PERMITISERVICES <br /> Oakland, CA 94611 <br /> FORMER MOBIL STATION 99CAS (AKA MARLER PROPERTY, and JH GRIFFIN MOBIL <br /> SERVICE), 75 EAST ALPINE AVENUE, STOCKTON, SAN JOAQUIN COUNTY <br /> (CASE#390857) <br /> The California Regional Water Quality Control Board-Central Valley Region (Central Valley <br /> Water Board) staff reviewed the Groundwater Monitoring and Remediation Status Report, First <br /> Quarter 2014 (Report) submitted on your behalf by Cardino ERI on 29 April 2014. Cardino ERI <br /> conducted groundwater monitoring on 19 and 20 March 2014. Results continue to show <br /> groundwater concentrations are not declining significantly, with Benzene at 6400 micrograms <br /> per Liter (ug/L), 5,200 ug/L; and 8,300 ug/L in MW-4, EX-1, and EX-2 respectively while under <br /> active soil and groundwater remediation. The water quality objective for benzene is 1 ug/L and <br /> the State Water Resources Control Board's Low Threat Closure Policy requires concentrations <br /> of benzene below 3,000 ug/L before regulatory closure of an underground storage tanks case <br /> may be considered. <br /> The soil vapor extraction (SVE) portion of the SVE/air sparging (AS)treatment system removed <br /> approximately 531 lbs. (80.5 gal.) of petroleum hydrocarbons during 62 days of operations in <br /> the first quarter of 2014, or 8.5 lbs. (1.3 gal.) per day. Since April 2012, SVE has removed <br /> approximately 12,320 lbs. (1,867 gal.) of TPH in soil. We are concerned the reported operation <br /> of the treatment system was less than 70% of the available run time, and petroleum <br /> hydrocarbons recovery was less than 2 gallons per day during the first quarter 2014 reporting <br /> period. Please submit a Work Plan to optimize the SVE/AS treatment system, or to enhance <br /> the existing system with additional technology(s), by 30 July 2014. <br /> Cardino ERI recommended continued operation of the SVE/AS treatment system and continued <br /> Quarterly Monitoring of monitoring wells DW-1, DW-2, EX-1, EX-2, MW-2, MW-4, and MW-5, <br /> with semiannual monitoring of MW-1, MW-3, and DW-3, and annual monitoring of MW-6 <br /> through MW-8, and DW-4. Horizontal and vertical delineation of the groundwater plume is <br /> defined at this site by: DW-1 through DW-4 are non-detect (ND) or slightly above detection <br /> limits (DW-1 Benzene, 0.52 ug/L), effectively delineating deeper impacts laterally as well as <br /> vertically. MW-6 (ND) delineates lateral extent to the north, MW-8 (ND) to the northeast, <br /> MW-7 (ND) to the southeast, MW-5 (Benzene, 1.0 ug/L)) effectively defines the pollution to the <br /> south, and MW-3 (ND) defines the extent of impacts to the west. Therefore, we concur with <br /> Cardino ERI's recommendations and believe that sufficient monitoring data exists to allow an <br /> additional reduction in the frequency of monitoring in the following wells: MW-1, MW-3, MW-5, <br /> DW-1, DW-2 and DW-3, to annual monitoring. The next quarterly groundwater monitoring and <br /> remediation status report is due 30 July 2013. <br /> KARL E. LONOLEY SCD, P.E., GHMR I PAMELA C. GREEDON P.E., BCEE, CXCCUTIVC Orriccn <br /> 11020 Sun Center Drive#200,Rancho Cordova,CA 85570 I www.waterboards.ca.gov/contralvalley - <br /> C,aecvcaeo veEEa <br />