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REMOVAL_2007
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PR0231227
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REMOVAL_2007
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Last modified
4/1/2020 11:59:31 AM
Creation date
11/6/2018 9:55:07 AM
Metadata
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Template:
EHD - Public
ProgramCode
2300 - Underground Storage Tank Program
File Section
REMOVAL
FileName_PostFix
2007
RECORD_ID
PR0231227
PE
2361
FACILITY_ID
FA0004033
FACILITY_NAME
BEST CALIFORNIA GAS LTD #172
STREET_NUMBER
7647
STREET_NAME
PACIFIC
STREET_TYPE
AVE
City
STOCKTON
Zip
95207
APN
07748014
CURRENT_STATUS
02
SITE_LOCATION
7647 PACIFIC AVE
P_LOCATION
01
P_DISTRICT
002
QC Status
Approved
Scanner
SJGOV\rtan
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FilePath
\MIGRATIONS\P\PACIFIC\7647\PR0231227\REMOVAL 2007 .PDF
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EHD - Public
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GeoHydrolagic Consultants Inc <br /> Michael Infurna of SJCEHD was present onsite during all well abandonment activities <br /> along with GHC staff. <br /> Existing well MW-12 was abandoned by over drilling on December 1, 2007, by Test <br /> America Drilling with a guide rod to make sure that the auger stayed true to the original <br /> borehole and the well was completely removed. MW-12 was overdrilled through the <br /> existing 12-inch diameter steel conductor casing using an 8.5-inch diameter O.D. hollow <br /> stem auger to total depth of 74 feet. The well was then filled with bentonite grout from <br /> the bottom of the borehole upward via 1-inch diameter tremie pipe.A total of 150 gallons <br /> of bentonite grout were placed in the borehole and topped with 4 bags of bentonite chips <br /> to a depth of approximately 16 feet below grade,which was up inside the steel conductor <br /> which was later removed during UST removal activities. <br /> Existing dual-nested well M W-11NW-3.was abandoned by over drilling on December 1, <br /> 2007, by Test America Drilling Co. with a guide rod to make sure that the auger stayed <br /> true to the original borehole and the well was completely removed. This well overdrilled <br /> through the existing 12-inch diameter steel conductor casing using a 10.5-inch diameter <br /> auger; however,the auger hooked on the steel conductor and was therefore switched out <br /> to an 8.5-inch diameter O.D. hollow stem auger in order to get through the conductor and <br /> the well was drilled out to a total depth of 61 feet.The well was then filled with bentonite <br /> grout from the bottom of the borehole upward via 1-inch diameter tremie pipe.A total of <br /> 150 gallons of bentonite grout were placed in the borehole and topped with 6 bags of <br /> bentonite chips to a depth of approximately 10 feet below grade, which was up inside the <br /> steel conductor which was later removed during UST removal activities. <br /> Existing dual-nested well VW-2 s,d was abandoned by over drilling on December 2, <br /> 2007, by Test America Drilling Co. with a guide rod to make sure that the auger stayed <br /> true to the original borehole and the well was completely removed. The well was <br /> overdrilled through the existing 12-inch diameter steel conductor casing using an 10.5- <br /> inch diameter O.D. hollow stem auger to total depth of 42 feet.The well was then filled <br /> with bentonite grout from the bottom of the borehole upward via 1-inch diameter tremie <br /> pipe.A total of 200 gallons of bentonite grout were placed in the borehole to a depth of <br /> approximately 5 feet below grade,which was up inside the steel conductor which was <br /> later removed during UST removal activities. <br /> 3.3 UST Removal Activities <br /> In September 2006,the contents of the UST were removed,the tanks and piping were <br /> triple rinsed,and appropriate measures were completed for in-place temporary closure of <br /> the three 12,000-gallon USTs and associated equipment.The liquid waste,approximately <br /> 900 gallons of rinsate, was transported by Asbury Environmental Services to <br /> DeMenno/Kerdoon of Compton, California where it was recycled. Copies of the waste <br /> manifest and recycling certificate are included in Appendix B.As noted on the SJCEHD <br /> Underground Storage Tank Disposition Tracking Record, on September 13,2006,the <br /> three 12,000 gallon USTs were decontaminated as a part of the temporary closure <br /> procedure(Appendix B). <br /> TOC 172 UST Removal Report Final Page 8 <br />
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