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Dennis Catanyag [EH] <br /> From: Mark Zollo [mzollo@lodi.gov] <br /> Sent: Monday, March 21, 2005 3:47 PM <br /> To: Dennis Catanyag [EH] <br /> Cc: Richard Prima; Dennis Callahan; Roger D. Rich; Ronald Bianchetti (E-mail) <br /> Subject: City of Lodi. 1331 S. Ham Ln., Cathodic Testing of 10K Gallon Unleaded Tank <br /> A ~JI <br /> RiserDetail.JPG D-A6Die1ec.JPG WasteONSump.JPG Un1eadSump2.JPG Un1eadSump1.JPG <br /> Dennis, <br /> Per your request: <br /> Regarding: 10,000 gallon unleaded tank cathodic protection (CP) system deficiency <br /> investigation. <br /> This summary begins from the engineer's (R. Bianchetti) and EHD's (D. Catanyag) <br /> <<RiserDetail.JPG>> <<D-A6Dielec.JPG>> <<WasteOilSump.JPG>> <<UnleadSump2.JPG>> <br /> <<UnleadSumpl.JPG>> last visit to the 1331 S. Ham Lane site on 3/4/05. At that time, Mr. <br /> Bianchetti detected continuity between the unleaded tank's cathodic system, the building's <br /> electrical system, and the Compressed natural gas (CNG) system, including the CNG's <br /> cathodic system. City of Lodi staff ordered a reference anode necessary for testing and <br /> spent last week investigating the various systems to locate the interconnection. This <br /> process turned out to be a bit tricky, but easily remedied. <br /> First, the as built plans from 1988 (D-A6Dielec.JPG & RiserDetail.JPG) indicate that <br /> both risers in the unleaded sump have dielectric fittings. One of the risers in the sump <br /> is the pump and the other was originally a mechanical tank fuel level gauge device. <br /> During the CNG project, the dispensers, the 10K gallon unleaded tank and the adjacent 2K <br /> gallon unleaded tank received upgrades and modifications. One of the modifications <br /> connected the two tanks by fiberglass piping using the riser that housed the mechanical <br /> tank level gauge (Tank level is measured electronically) . A copper line connected to the <br /> pump housing utilizes vacuum created during pump operation to maintain a siphon between <br /> the tanks. Although the risers did not share continuity, we were unable to ascertain <br /> which of the risers connected to the tank without a dielectric fitting since we could not <br /> test between the tank body and the risers. <br /> A review of file information by the Steel Tank Institute provided a simple method to <br /> positively test continuity between the tank and the risers by attaching a screw with a <br /> wire lead to the end of the tank gauge stick. The stick is dropped into the interstitial <br /> space of the tank and contacts the tank's metal interior. A Lodi Electric Utility (LEU) <br /> technician determined that the pump riser was insulated from the tank by a dielectric <br /> fitting and that the siphon riser was not. <br /> This determination indicated two problems with the CP system. First, The CP system <br /> was connected (clamped) to the fuel pump riser. Second, the two risers were electrically <br /> connected by the copper siphon line. The solution was to move the CP system clamp to the <br /> siphon riser, which is directly connected to the tank and to use non-conductive tubing for <br /> the siphon line (UnLeadSumpl.JPG & UnLeadSump2.JPG) . These two changes isolate the pump's <br /> electrical system from the tank and the tank's CP system. Readings by the LEU technician <br /> showed immediate and satisfactory CP system performance. This faulty configuration of the <br /> 10K gallon unleaded tank CP system was the interconnection that Mr. Bianchetti detected on <br /> his last visit and is due to work performed by Stockton Service Station Equipment Co. in <br /> the course of the CNG project (1/02 through 12/02) , not a long term deficiency with the CP <br /> system. <br /> Mr. Bianchetti has tentatively scheduled this Friday to perform the retest of the <br /> 10K tank and begin some work on the CNG CP system. If the tank test satisfactorily, which <br /> I expect, I would estimate a finished report within a week (+/-) . <br /> The last image shows the installed test board for the waste oil tank <br /> (WasteOilSump.JPG) , which corrected the problem with that tank's CP system. <br /> 1 <br />