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ARCHIVED REPORTS XR0000449
EnvironmentalHealth
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EHD Program Facility Records by Street Name
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BENJAMIN HOLT
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2908
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3500 - Local Oversight Program
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PR0544111
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ARCHIVED REPORTS XR0000449
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Last modified
2/7/2019 3:35:41 PM
Creation date
2/7/2019 2:05:35 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0000449
RECORD_ID
PR0544111
PE
3528
FACILITY_ID
FA0003625
FACILITY_NAME
ARCO STATION #83560*
STREET_NUMBER
2908
Direction
W
STREET_NAME
BENJAMIN HOLT
STREET_TYPE
DR
City
STOCKTON
Zip
95207
APN
09763032
CURRENT_STATUS
02
SITE_LOCATION
2908 W BENJAMIN HOLT DR
P_LOCATION
01
P_DISTRICT
002
QC Status
Approved
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EHD - Public
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. ARCO PRODUCTS COMPANY SOIL VAPOR EXTRACTION AND <br /> EATMENT (SVETS) AND AIR SPARGING (AS) SYSTEMS OPERATING REPORT <br /> First Quarter 1997 <br /> Facility 4 2133 <br /> Facility address 2908 Benjamin Holt Dr Stockton,CA <br /> ARCO engineer Mr Paul Supple <br /> Consultant[project manager] Brown and Caldwell (Steve Misner,(916)444-0123] <br /> Lead agency San Joaquin County Health Department <br /> Reporting period 12/31196-3/31197 <br /> Equipment inventory Atrex KATOX 100 <br /> catalyst module <br /> 10 hp Baldor Motor 240VAC/1 phase <br /> Gast Oilless Regenerative Blower <br /> ATI telemetry system <br /> Knockout pot <br /> MD Pneumatics sparge blower <br /> The SVETS was not operated this quarter due to low influent concentrations to the oxidizer as a result <br /> of high groundwater levels The SVETS was started briefly on 1/13/9'7 to check influent concentrations <br /> which were 8 2 ppm following 2 hours of operation The air sparge system is fully operational and <br /> operated 100%for the reporting period <br /> Operating mode Catalytic Oxidation <br /> AQMD Permit##,AIN N-78-3-0 <br /> End of period date 3/31197 <br /> TPH conc end of period(PID, ppmv) 8 2 (1/13197) <br /> Benzene conc end of period(Lab,ppmv) -- <br /> Flowrate end of period -- <br /> TPH destroyed this period(PID, lbs) 0 <br /> Utility usage <br /> Electric(KWH) 94 <br /> Operating hours this period 0 <br /> Percent up time 0% <br /> Operating hours to date 8112 <br /> "--"Not available or not applicable <br /> Attachments <br /> Table 1 Soil Vapor Extraction and Treatment System Influent Data <br /> Table 2 Soil Vapor Extraction and Treatment System Effluent Data <br /> ko Table 3 Soil Vapor Extraction Well Data <br /> Table 4 Air Sparging Well Data <br /> Table 5 Dissolved Oxygen Concentrations <br /> Chart 1 TPH-G Concentrations vs Time <br /> Chart 2 Cumulative Hydrocarbons(as TPH-G)Removed vs Time <br />
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