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ARCHIVED REPORTS XR0000885
EnvironmentalHealth
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3500 - Local Oversight Program
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PR0544147
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ARCHIVED REPORTS XR0000885
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Last modified
2/14/2019 2:04:39 PM
Creation date
2/14/2019 1:15:12 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0000885
RECORD_ID
PR0544147
PE
3526
FACILITY_ID
FA0004522
FACILITY_NAME
SKIPS SERVICE STATION
STREET_NUMBER
300
Direction
S
STREET_NAME
CALIFORNIA
STREET_TYPE
ST
City
STOCKTON
Zip
95206
APN
14909501
CURRENT_STATUS
02
SITE_LOCATION
300 S CALIFORNIA ST
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
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EHD - Public
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r <br /> On May 2 and 3, 2000 the soil borings for both MW#5 and MW46 were made as described in the <br /> work plan of 3/17/2000.Monitoring wells were installed in both of these soil bores. The work plan <br /> of 3/17/2000 also included a soil bore and monitoring well (MW#4)to be installed in the sidewalk <br /> on the north side of Lafayette Street. This soil bore was not completed as planned. An unknown <br /> underground storage tank was encountered in the direct path of the soil bore. As a result of this <br /> encounter, the soil bore was abandoned and the local agencies were notified. <br /> CPT#3 was installed on June 13,2000 in the Caltrans right of way. This CPT is northeast of the site, <br /> and the data gathered is in the report issued for that work. <br /> All monitoring wells have been sampled quarterly, and a recap of the findings is attached. <br /> A work plan to expand the horizontal definition of the contamination plume was approved in <br /> December of 2000.This work plan called for the installation of three new CPT's within the Caltrans <br /> R/W to the north of the project site. These CPT's were completed on March 8, 2001 and soil and <br /> water samples were extracted to a depth of 125 feet. Also, included in the work plan of December <br /> 2000 was the installation and testing of four new monitoring wells,(MW-8S,MW-8D,MW-7,MW- <br /> 9) to be placed on the project site or the adjacent property. These monitoring wells were completed <br /> on April 11, 2001. <br /> In January of 2002 the owners of this property removed the apartment house structure on the east <br /> side of the property. At the time of this report that portion of the property is clear without any <br /> structures or other improvements. In April of 2002 the author submitted a work plan for the <br /> installation of an extraction well with a pump test to determine the viability of a pump and treat <br /> remediation system. <br /> On August 9 & 10, 2002 the extraction well installed for the pump test was completed and <br /> developed. <br /> REPORT OF FINDINGS FOR THE FOURTH QUARTER 2002 MONITORING EVENT <br /> Procedure <br /> On December 30,2002,Del Tech Geotechnical Support Services extracted water samples from all <br /> of the monitoring wells on the above stated property, with the exception of MW-8D & MW-8S. <br /> MW-81) & MW-8S were damaged and covered with soil from the clearing of all buildings on the <br /> property to the east of the site. These wells were found by the GPS coordinates and marked for <br /> future repair.The work was supervised by Foothill Engineering. Some of the monitoring wells were <br /> in need of maintenance with missing locks and low grout column. All of the monitoring wells,with <br /> the exception of MW-8D &MWBS, were repaired and new locks were in stalled. <br /> All samples were extracted using the tube with check valve pump system. Purge rates were+/- .5 <br /> g.p.m. and the physical properties of the groundwater can be found in the Del-Tech Field Report <br /> which is attached and part of this report. <br /> The replacement and original monitoring wells were sampled for analysis, with the exception of <br /> MW-2R which was dry. The original monitoring wells (MW-1, MW-2, MW-3) were used to <br /> establish the groundwater elevation and hydraulic gradient. All samples were transported under <br /> chain of custody to Sherwood Labs of Hilmar, California for analysis by EPA method SW8020F. <br /> Samples were transported under chain of custody to Entech Analytical Labs for analysis by EPA <br /> 2 <br />
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