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ARCHIVED REPORTS XR0001225
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PR0536689
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ARCHIVED REPORTS XR0001225
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Entry Properties
Last modified
3/4/2019 5:24:59 PM
Creation date
3/4/2019 1:06:57 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0001225
RECORD_ID
PR0536689
PE
2957
FACILITY_ID
FA0021073
FACILITY_NAME
STKN CHARTER WAY COMMINGLED PLUME
STREET_NUMBER
508
Direction
W
STREET_NAME
CHARTER
STREET_TYPE
WAY
City
STOCKTON
Zip
95206
APN
16504016
CURRENT_STATUS
01
SITE_LOCATION
508 W CHARTER WAY
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
Scanner
WNg
Tags
EHD - Public
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S [EC0R <br /> Conceptual Site Model <br /> March 24, 2004 <br /> Page 13 <br /> 4AvE <br /> B <br /> pounds (approximately 1,600 gallons) of TPHg from January 1997 to February 1998 The SVE <br /> system was shut down due to decreasing concentrations (Delta, 2000) <br /> 633 Historical Report Summary <br /> In July 1991, a subsurface investigation consisting of four soil borings, was conducted at former ; <br /> Arco service station 2168 to evaluate the extent of hydrocarbons in the soil and groundwater <br /> Samples were analyzed for TPHg and BTEX TPHg concentrations ranged from 40 mg/kg (S-25-131) y` <br /> to 2 1 mg/kg (S-30-131), benzene ranged from 0 46 mg/kg (S-25-131) to 0 0059 mg/kg (S-40-132) f <br /> These activities are summarized in Resna's April 7, 1992 Addendum to Work plan for Subsurface y <br /> Investigation <br /> sit <br /> In 1993, Resna reported that dissolved hydrocarbons in the deeper zone were the result of off-site <br /> migration and proposed to conduct an off-site investigation as reported in Resna's June 9, 1993 <br /> Status of Environmental Investigation, First Quarter 1993, and Addendum to Work Plan <br /> k <br /> In October of 1993, A Resna field geologist supervised Westex Drilling, as they completed two offsite <br /> b� <br /> soil borings (B-20 and B-21) Soil borings B-20 and B-21 were converted to groundwater monitoring a <br /> wells and renamed MW-6 and MW-7 Resna reported that analytical results obtained from samples <br /> collected from MW-6 and MW-7 indicated a possible source of hydrocarbons up-gradient of the <br /> ARCO site Groundwater samples collected from MW-6 reported maximum TPHg and benzene <br /> concentrations of 93,000 pg/L and 15,000 pg/L, respectively TPHg and benzene were reported at <br /> concentrations of 42,000 pglL and 3,100, respectively in MW-7 These activities are summarized in <br /> Resna's February 15, 1994 Status Report Fourth Quarter <br /> In January 1997 EMCON installed and began operating a soil vapor extraction (SVE) and treatment <br /> system Influent and effluent samples were collected and submitted for chemical analysis Vapor <br /> samples were analyzed for TPHg and BTEX TPHg and BTEX influent concentrations were 55,000 <br /> milligrams per cubic meter (mg/m), 980 mg/m3, 1,400 mg/m3, 200 mg/m3, and 890 mg/m3, Y' <br /> respectively These activities are summarized in EMCON's February 13, 1997 Source Test Results <br /> for the Soil Vapor Extraction and Abatement System report <br /> In February of 1998, EMCON shut down the SVE and treatment system for a three week period to <br /> allow for the soil vapor concentrations to rebound Prior to the system being turned off background ; <br /> influent vapor samples were collected The SVE system was restarted three weeks after system <br /> shut-down and influent vapor samples were collected and submitted for chemical analysis <br /> Continued monitoring indicated a decrease in TPHg and benzene levels over a few days Based on <br /> field and analytical data EMCON shut down the SVE system These activities are summarized in fi <br /> EMCON's April 8, 1998 letter, Results of Soil Vapor Extraction and Assessment <br /> Between July and August 2000, Delta environmental installed five groundwater monitoring wells on r <br /> site (MW-1B, MW-1C, MW-8, MW-86, and MW-8C) MW-113 and MW-1C were installed adjacent to <br /> MW-1 MW-8, MW-8B, and MW-8C were installed up gradient of the former UST's The reported <br /> purpose of the clustered wells was to establish vertical characterization of groundwater quality by <br /> collecting samples from screened intervals at discrete depth intervals These activities are <br /> summarized in Delta Environmental Consultants, Inc November 22, 2000 Soft and Groundwater <br /> 9 <br /> Investigation Report <br /> 11Chevron1920331REPC)RTSICSM%CSM 92033(REV B) doc <br /> 1 <br /> i <br />
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