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CAMBRIA <br /> Previous Work <br /> 1994 UST Removal During December 1994, four single-walled steel USTs (two 10,000-gallon <br /> and two 6,000-gallon) and associated product piping were removed Petroleum hydrocarbons <br /> were detected in soil samples collected from beneath the former dispenser islands and product <br /> piping and in the southeastern half of the UST excavation Fugro West, Inc (Fugro) of <br /> Roseville, California performed over-excavation beneath the dispenser area and UST complex <br /> and collected additional soil samples One soil sample collected from the bottom of the UST <br /> excavation contained 1,000 parts per million (ppm) total petroleum hydrocarbons as gasoline <br /> (TPHg), and one soil sample collected from the northern sidewall of the dispenser excavation <br /> contained 2 7 ppm TPHg Complete results of the UST removal are documented in the Fugro <br /> April 19, 1995 Underground Storage Tank Closure Report <br /> 1996 Sod Borings During February 1996, Enviros, Inc (Enviros)drilled two GeoProbeo borings <br /> (GP-1 and GP-2) in the vicinity of the UST complex to investigate the extent of petroleum <br /> hydrocarbons detected during the December 1994 tank removal activities Enviros drilled one <br /> angle boring (GP-2) beneath the UST complex and one vertical boring (GP-1) adjacent to the <br /> UST complex Soil samples collected from the two borings did not contain detectable <br /> concentrations of petroleum hydrocarbons but did contain methyl tertiary butyl ether (MTBE) at <br /> concentrations up to 29 ppm This investigation is described in Enviros' May 8, 1996 Soil <br /> Boring Installation Report <br /> 1999 Soil Barings During January 1999, Cambria drilled five soil borings (SB-1 through S13-5) <br /> in the vicinity of the UST complex TPHg was only detected in boring S13-3 at a concentration <br /> of 3 17 ppm No benzene was detected in any of the soil borings MTBE was detected (by EPA <br /> Method 8260) in all borings at concentrations ranging from 0 00807 to 92 9 ppm Groundwater <br /> samples were collected from borings SB-3 and S134 They contained 46,000 and 6,610 parts per <br /> billion (ppb) TPHg, 243 and 63 6 ppb benzene, and 28,000 and 8,050 ppb MTBE, respectively <br /> These results are summarized in Cambria's June 9, 1999 Site Investigation Report <br /> 1999 Well Installation During November 1999, Cambria drilled four soil borings (GP-3 through <br /> GP-6) and installed three groundwater monitoring wells (MW-1, MW-2, and MW-3) at this site <br /> The soil borings were drilled in the vicinity of the dispenser islands to determine if this was the <br /> source area Analytical data collected from the borings suggested the dispenser islands were not <br /> the source area The monitoring wells were installed around the UST complex (Figure 2) <br /> Groundwater samples collected from these wells contained TPHg, benzene, and MTBE <br /> • Analytical data from these wells and from previous soil borings drilled in the UST area <br /> suggested the USTs are likely the primary source area for petroleum hydrocarbons and MTBE <br /> 0955 2 <br />