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3500 - Local Oversight Program
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PR0544475
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SITE INFORMATION AND CORRESPONDENCE
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Last modified
5/17/2019 3:43:21 PM
Creation date
5/17/2019 3:10:19 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
SITE INFORMATION AND CORRESPONDENCE
RECORD_ID
PR0544475
PE
3528
FACILITY_ID
FA0003602
FACILITY_NAME
TESORO (SHELL) 68151
STREET_NUMBER
35
Direction
N
STREET_NAME
CHEROKEE
STREET_TYPE
LN
City
LODI
Zip
95240
APN
04318003
CURRENT_STATUS
02
SITE_LOCATION
35 N CHEROKEE LN
P_LOCATION
02
P_DISTRICT
004
QC Status
Approved
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EHD - Public
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I L L 1 4l3 1J�. r. �v s �..y i✓ v i u .0 u c....r v v i <br /> 'ILIEM0RANDUM �--' <br /> CALIFORNIA REGIONAL WATER QUALITY CONTROL BOARD a CENTRAL VALLEV REGION <br /> 3443 Routier Road,Suite A Phone: (916)255-3000 <br /> Sacramento,California 95827-3098 CALNET: 8494-3000 <br /> TO. EAT,GLB FRQ:12 SDT <br /> Underground Thn1c Unit Underground Tank Unit <br /> BATE: b October 1995 SIGNATURE: <br /> SUBJECT. REQUEST OR CLOSURE,BEACON,STATION,35 Nj)RTH CHFJRofEE LANE, <br /> J,OVI, SAN JOAQUIN COUNTY <br /> We received a request for closure dated June 1995,prepared by Delta Environmental Consultants, <br /> Inc.(Delta). The report and file contain all the information required in Appendix B,with the <br /> exception of calculations and figures showing the cone of influence for the vapor extraction <br /> system. Five monitoring wells remain on-site. <br /> In September 1986,a 10,000 gallon diesel tank was removed from the site and five monitoring <br /> wells installed. The investigation revealed soil and ground water contamination and a vapor <br /> extraction system(VES)was installed in September 1987_ Delta's report states that the VES was <br /> in operation in October and November 1989,and September through December 1992. l iowever, <br /> no explanation has been provided for the sporadic operation of the system. San Joaquin County <br /> wrote a letter to Ultramar, Inc.dated 6 April 1995,stating that the VIES was operated from <br /> October 1989 to February 1993. The VES consisted of four VE wells,which were abandoned in <br /> 1995,during tank removal,and MW-2 and MW4. <br /> In February 1995,three unleaded gasoline tanks,two 12,000 gallon and one 10,000 gallon,wore <br /> removed from the site and contaminated soil was over excavated to 16 feet below ground surface <br /> (bgs)with a small area excavated to 26 feet bgs. The County letter states that no further remedial <br /> action is warranted based on the excavation sample results. The confirmation samples revealed up <br /> its 16 parts per billion(ppb)ethylbenrene and 200 ppb xylenes at 26 feet hgs remain in soil. No <br /> confirmation samples were taken from the north end of the excavation where a previous sample <br /> revealed 1,100 parts per million Total Petroleum Hydrocarbons as gasoline('1711g)at 15 feet bgs. <br /> Ground water monitoring showed concentrations tip to 3,750 ppb TPIig and 33, 157,235 and 550 <br /> ppb benzene,toluene,ethylbenzene and xylenes,respectively,in 1986. In July 1989,all five wells <br /> were contaminated. The extent of ground water contamination was never completely dclined, <br /> however,following startup of the VES,concentrations in ground water declined. Six ground <br /> water monitoring events have been performed since March 1990. All samples were non-detect <br /> with the exception of 0.6 ppb benzene in June 1990,in MW-1,which has not been sampled:+ince <br /> because of low water levels,and 68 ppb gasoline in MW-4 in May 1992. <br /> Upon receipt of the calculations and/or contours of the zone of influence and operation times for <br /> the VES,staff can reconsider Ultramar's request for no further action, <br /> SI)J <br />
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