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S E C ® R <br /> In 1991, three 10,000-gallon USTs and four 2,000-gallon USTs were removed The <br /> USTs were replaced with those that currently exist at the site (three 10,000-gallon <br /> gasoline USTs) Well MW-2 was destroyed during UST removal activities (GRI, <br /> Groundwater Monitoring Well, CPT, and Ozone Microsparge System Installation Report, <br /> May 9, 2003) <br /> In 1992, a hydropunch study and a soil vapor extraction (SVE) test were conducted <br /> The SVE test was conducted over a six-hour period on January 21, 1992 Results of the <br /> SVE test indicated that a 100-standard cubic feet per minute (scfm) air flow rate was <br /> sufficient to achieve an 85-foot radius of influence (IT, Soil Extraction Pilot Test, March <br /> 1992) <br /> Between November 16, 2000 and January 2, 2001, eight weekly groundwater extraction <br /> events were performed During each event, approximately 2,400 to 3,800 gallons of <br /> groundwater were removed from well MW-3 In addition, approximately 600 gallons of <br /> groundwater were removed from well MW-7 on November 16, 2000 A total of <br /> approximately 27,200 gallons of groundwater were removed from beneath the site Based <br /> on the results of groundwater samples periodically collected from well MW-3 prior to and <br /> following each of the extraction events, an estimated total of 26 63 pounds of methyl <br /> tertiary butyl ether (MtBE) were removed from beneath the site The weekly groundwater <br /> batch extraction activities were discontinued following the receipt of approval from the <br /> San Joaquin County Environmental Health Division (SJCEHD) <br /> In April 2001, GRI supervised the drilling of eight Geoprobe soil borings (B-1 through B- <br /> 8) at and in the vicinity of the site, and one cone penetrometer test (CPT) boring on-site r <br /> (CPT-1) Concentrations of petroleum hydrocarbons and fuel oxygenates were not <br /> detected in the soil from the CPT boring, and in groundwater samples collected from <br /> borings B-3, B-5, B-6, B-7, and B-8 MtBE was detected in groundwater samples from <br /> borings B-1, B-2, B-4, and the 75-foot groundwater sample from CPT-1 up to a 14 <br /> maximum concentration of 120 micrograms per Liter (pg/L) Concentrations of di- <br /> isopropyl ether (DIPS) and 1,2-dlchloroethane (1,2-DCA) were also detected in <br /> groundwater from borings B-1 and CPT-1, respectively (GRI, Subsurface Investigation <br /> Report, June 2001) <br /> On August 8, 9, and 10, 2001, GRI supervised the installation of three off-site and one <br /> on-site groundwater monitoring well (MW-8 through MW-11) With the exception of a <br /> concentration of MtBE in a 14-foot soil sample from boring MW-11 (1 7 ppm) and a <br /> concentration of MtBE in the groundwater sample from well MW-11 (110 parts per billion 4� <br /> [ppb]), soil and groundwater samples did not contain detectable concentrations of <br /> contaminants (GRI, Monitoring Well Installation Report, September 2001) <br /> Between December 3 and 7, 2001, SECOR International Incorporated (SECOR) ?� <br /> performed dual-phase extraction (DPE) testing at the site The DPE test was performed <br /> on wells MW-3 and MW-7 over a 110-hour period Flow rates during the test vaned from <br /> 10 90 to 33 41 scfm, and vacuum rates varied from 24 to 25 inches of mercury (in Hg) <br /> Over the course of the five-day event, SECOR reportedly removed a total of 0 pounds <br /> (Ibs) of TPHg, 0 01 lbs of benzene, and 6 64 lbs of MtBE SECOR determined that the <br /> vacuum radius of Influence was between 36 and 60 feet Approximately 20,830 gallons <br /> of groundwater were extracted during the DPE event Based on the low mass removal <br /> • achieved with this test, SECOR concluded that DPE was not an effective remedial ,, <br /> ri <br /> k <br /> 1ConocoPhdhpslRetai1 Sites1111921QSSR12005=2005 QSSR and QRPS doe h <br /> ' s <br /> i <br />