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FIGURE 813 <br /> • Figure 813 represents the TBA plume in the B zone TBA was previously evident in wells <br /> MW613 and 8B at 10 and 7 7 ug/L respectively, currently TBA is below laboratory lower <br /> detection limts of 5 ug/L <br /> Figure 9 illustrates the subsurface lithology and the extent of the A and B zones <br /> groundwater plumes within the A and B zones <br /> SUMMARY AND RECOMMENDATIONS <br /> The City of Stockton Department of Municipal Utilities in a letter addressed to Mary <br /> Sanchez, dated October 8 2004 gave notice of intent to hold Mary Sanchez liable for <br /> costs of mitigating contamination that is encountered during the construction of a trunk <br /> sewer line along Country Club Blvd San Joaquin County Health approved a workplan <br /> submitted by Western Geo-Engineers to install a pump into well MW10 The City of <br /> Stockton Municipal Utilities Department has granted a permit to discharge treated <br /> pumped water from well MW10 to the sanitary sewer at a rate not to exceed 10 gallons <br /> per minute Groundwater pumping from MW10 commenced on April 8, 2005 with <br /> discharge to sewer (7 gpm) occurring at that time The City of Stockton construction of <br /> the sewer line came near the site on April 27, 2005 The groundwater pump and <br /> treatment system was turned off on May 10, 2005 due to the presence of TBA (7 1 ug/L) <br /> in the discharge to sewer A request to modify the treatment system was drafted and <br /> • submitted to the City of Stockton Department of Municipal Utilities on May 23, 2005 <br /> Completion of the treatment system modification was completed on August 25, 2005 and <br /> the system was tested on that date, pumping 751 gallons from MW10 through the <br /> treatment system into a 22,000 gallon capacity Baker Tank, with no discharge to sewer <br /> The carbon units were subjected to high pressure (greater than 12 psi) and the system was <br /> shut down to determine the cause of the high pressure It was felt that the restriction from <br /> the water totalizer may have caused the high pressure, the system was restarted without <br /> the totalizer in the the system, but the high pressure persisted It was discovered that the <br /> discharge line from the last carbon unit (carbon ##5) was partially clogged, restricting the <br /> flow to the Baker Tank The clog was removed and the pump and treatment system <br /> restarted on September 1, 2005 The Baker Tank, high level float switch was activated <br /> after 16,911 gallons of groundwater had been pumped from MW10 and treated through <br /> the carbon/aeration system Samples of this treated and stored water showed that this <br /> water met sewer discharge requirements and was discharged to the sanitary sewer on <br /> September 21 through 23, 2005 at a rate of 5 gpm To determine the influence that <br /> pumping from MW10 was having on surrounding wells, depth to water measurements <br /> were obtained prior to pumping, prior to termination of pumping and five days after <br /> termination of pumping at a rate of 8 9 gpm from September 28 through October 5, 2005 <br /> 16,623 gallons were pumped from MW10, treated through the carbon/aeration system <br /> and stored in the Baker Tank during that time Charts developed from the depth to water <br /> measurements show that pumping from MW10 at a rate of 8 9 gpm influences the <br /> Country Club Food and Fuel wells A second pump influence test is scheduled for <br /> October 2005 at a rate of 5 gpm <br /> 11 Sanchez QM 3`d <br /> 2005 <br />