Laserfiche WebLink
fiom well MW10 is most likely pulling the MtBE plume from CCFF onto the Sanchez <br /> . property, thus removing MtBE from both sites while pumping is occurring <br /> FIGURE 7B <br /> Figure 7B represents the MtBE plume in the B zone Figure 7B resembles figure 7A with <br /> the only difference being an increase in MtBE found at well 6B Historic water samples <br /> obtained from piezometers PZIB and PZ2B contained 78 and 21 ug/L respectively <br /> TBA <br /> FIGURE 8A <br /> Figure 8A represents the TBA plume in the A zone TBA is only evident in well MWBA <br /> at 6 1 ug/L Historically TBA was detected in "GeoProbe" holes P8 and P10 at 11 and 6 <br /> ug/L respectively (February 2001) <br /> Figure 9 illustrates the subsurface hthology and the extent of the A and B zones <br /> groundwater plumes within the A and B zones <br /> . SUMMARY AND RECOMMENDATIONS <br /> The City of Stockton Department of Municipal Utilities in a letter addressed to Mary <br /> Sanchez, dated October 8 2004 gave notice of intent to hold Mary Sanchez liable for <br /> costs of mitigating contamination that is encountered during the construction of a trunk <br /> sewer line along Country Club Blvd San Joaquin County Health approved a workplan <br /> submitted by Western Geo-Engineers to install a pump into well MW10 The City of <br /> Stockton Municipal Utilities Department has granted a permit to discharge treated <br /> pumped water from well MW 10 to the sanitary sewer at a rate not to exceed 10 gallons <br /> per minute Groundwater pumping from MW10 commenced on April 8, 2005 with <br /> discharge to sewer (7 gpm) occurring at that time The City of Stockton construction of <br /> the sewer line came near the site on April 27, 2005 The groundwater pump and <br /> treatment system was turned off on May 10, 2005 due to the presence of TBA (7 1 ug/L) <br /> in the discharge to sewer A request to modify the treatment system was drafted and <br /> submitted to the City of Stockton Department of Municipal Utilities on May 23, 2005 <br /> Completion of the treatment system modification was completed on August 25, 2005 and <br /> the system was tested on that date, pumping 751 gallons from MW10 through the <br /> treatment system into a 22,000 gallon capacity Baker Tank, with no discharge to sewer <br /> The pump and treatment system was restarted on September 1, 2005 The Baker Tank, <br /> high level float switch was activated after 16,911 gallons of groundwater had been <br /> pumped from MW10 and treated through the carbon/aeration system Samples of this <br /> treated and stored water showed that this water met sewer discharge requirements and <br /> was discharged to the sanitary sewer on September 21 through 23, 2005 at a rate of 5 <br /> gpm To determine the influence that pumping from MW10 was having on surrounding <br /> 11 Sanchez QM 4t1' 2005 <br />