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<br /> TWO.:Gro111a water Extraction Masa Remoyal'I?ata, +a�er ShelllS,tzyt !$Ilalxsan�25751
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<br /> TPH9 Benzene MTBE
<br /> Site Row Meter Cumulative Row TPHg Penod Cumulative Benzene Period Cumulative MTBE Penod Cumulative
<br /> Visit Reading Volume Rate Conc Removal Removal Conc Removal Removal Conc Removal Removal Active
<br /> mmld ) al ( (RDW b) (pounds) (pounds) b (pounds) ( n&) ( b) ds) (pounds) Wells Comments
<br /> 05131/01 20 0 0 0 0 RW-lA Startup samples taken
<br /> 05/31/03 220 200 36,000 0.060 0060 9,400 0016 0016 63,000 0105 0105 RW-lA
<br /> Continuous groundwater extraction and
<br /> 0680101 290 270 000 3,000 0 002 0 062 650 0 000 0 016 4800 0 002 0 107 RW-1A sewer discharge began
<br /> 06/25/01 6,950 6,930 093 28,D00 156 162 5,700 0 317 0 333 16,000 0 889 0 996 RW-1A
<br /> 07/16/01 8,222 8,202 004 34 000 0 361 198 9,800 0104 0 437 61,000 0 647 164 RW-lA
<br /> 07123!01 16,610 16,590 083 23,000 161 359 4 600 0 322 0 759 330D0 131 395 RW-1A
<br /> 081=1 31,200 31,180 101 47,000 572 931 121000 146 222 87,000 106 145 RW-tA
<br /> 0880/01 33,320 33,300 008 44,000 0778 101 111000 0195 241 99,000 175 163 RW-lA
<br /> 09/06101 67,750 67,730 141 50,000 144 245 10,000 287 529 110,000 316 479 RW-1 A
<br /> 09/21/01 96 310 96,290 132 53,000 126 371 9,800 234 762 110,000 262 741 RW-1A
<br /> 10/03/01 98,030 98,010 010 47,000 0 675 378 12,00D 0172 780 15D,DD0 215 763 RW-1A
<br /> 10/16/0! 100,400 100,380 013 45,000 0 890 386 12,000 0 237 $03 200,000 396 802 RW-1 A
<br /> Carbon chaageout pelfomied on l 111101
<br /> System downtime spprox mately 12
<br /> I IID8101 104340 104,320 0 t2 <50,000 0 822 395 12,000 0 395 843 I60,000 526 955 RW-1 A hours
<br /> 11/21/01 109,740 109,720 029 33,000 IA!) 410 9,000 0406 883 110000 496 90A RW IA
<br /> 12/12/01 111,t t0 111,090 005 120,000 137 423 9,700 0 111 894 120,000 137 918 RW-lA
<br /> 1228101 168,190 168,170 248 33,000 1572 580 81600 4 096 1304 98 000 4668 t38 5 RW-lA
<br /> System down due to damaged power
<br /> 01126102 322,220 322,200 369 55,000 7069 1287 9,300 11 953 2499 91,000 11696 2554 RW-lA lines Re-started 1/10102
<br /> Cafta ehaageout performed on 2112/02
<br /> System downtime approximately 24
<br /> 0222102 449,770 449,750 328 63,000 6705 1958 7,900 8 408 3340 78,000 8302 3385 RW lA hours
<br /> 03/06102 513,2W 513,180 367 13,000 688 202.7 1,400 0741 3414 11,000 532 3443 RW-lA
<br /> 03/27/02 569,340 569,320 136 NS 2389 2266 NS 3 513 3766 NS 3701 3813 RW-1A
<br /> 04/01/02 587,495 587,475 252 51,000 773 2343 7,500 1136 3879 79,000 1197 3933 RW-lA System honed off 411 and m1arted 4/23
<br /> 04125/02 595,400 595,380 023 44,000 2.90 2372 7,200 0 475 3927 87,000 574 3990 RW-1A Carbon changeait pafattrted as 4117
<br /> 102
<br /> 0582/02 679 800 679,780 217 57,000 4014 2773 7,500 5 282 4455 69,000 4859 44715 RW-1A
<br /> ON 19102 769.900 769,880 223 86,000 6465 347-0 7,800 5 864 5041 62,000 4661 4942 RW l A
<br /> 06126102 794,831 794 811 2 47 60,000 12.48 3141 61900 1435 51.85 66,000 1373 5079 RW-lA Carbon changeatit performed on 7/17/02
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