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ARCHIVED REPORTS FIRST QUARTER GROUNDWATER MONITORING REPORT FEBRUARY 2014
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PR0009276
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ARCHIVED REPORTS FIRST QUARTER GROUNDWATER MONITORING REPORT FEBRUARY 2014
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Last modified
6/25/2019 8:44:12 AM
Creation date
6/25/2019 8:18:44 AM
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EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
FIRST QUARTER GROUNDWATER MONITORING REPORT FEBRUARY 2014
RECORD_ID
PR0009276
PE
2960
FACILITY_ID
FA0012033
FACILITY_NAME
PILKINGTON NORTH AMERICA
STREET_NUMBER
500
Direction
E
STREET_NAME
LOUISE
STREET_TYPE
AVE
City
LATHROP
Zip
95330
APN
19812008
CURRENT_STATUS
01
SITE_LOCATION
500 E LOUISE AVE
P_LOCATION
07
P_DISTRICT
003
QC Status
Approved
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' Table B - Historic Diesel Thickness Measurements and Product Recovery Data(06118/99 through 3131/14) <br /> Depth[o Cumulative <br /> Date Recovery Floating Depthm Diesel Diesel Operations and Maintenance Notes <br /> Well Diesel Groundwater Thickness Removed <br /> ' (gallons) <br /> RW-2 13.06 13.12 0.06 19.70 The skimmer pump regulator and battery were not operational.The line pressure was <br /> functional;however,the tank pressure was not.Absorbent sacks in RW-2 and RW-4 <br /> 4/13.03 RW-3 13.19 13.39 0.30 2.80 strained;a negligible amount of product recovered.Skimmer pump removed from RW-3 <br /> ' and installed in RW-4.Recovery socks were reinserted in RW-2 and RW-3. <br /> RW-4 12.02 15.58 3.56 42.45 Approximately 3.5 gallons in product recovery barrel. <br /> RW-2 13.06 13.14 0.08 19.70 Skimmer ptanp removed from RW4 and inspected.Skimmer pump was reinstalled in RW <br /> 4 and the pump cycle act at(6)5-minute cyclesiday.The N2 tank supply tank and battery <br /> ,_03 RW-3 13.02 13.51 0.49 2.80 were replaced and a new regulator was purchased and installed.The pump cycle was reset <br /> at(3)3-minute cycles per day.Absorbent socks in RW-2 and RW-3 stmined and <br /> RW-4 12.58 13.05 0.47 49.45 replaced;a negligible amount of product recovered.Approximately 10.5 gallons in <br /> product recovery barrel. <br /> ' RW-2 13.16 13.37 0.21 19.70 Initial measurement of the product recovery barrel indicated approximately 22.75 gallons <br /> of diesel product.Skimmer pump left in RW-4:pump cycle reset to(I)5-minute <br /> 522/03 RW-3 13.02 14.34 1.32 3.80 cycldday.Absorbent socks in RW-2 and RW-3 removed and strained;a negligible <br /> ' amount of product recovered.Approximately I gallon of free product was bailed from <br /> RW-3 and added in the product recovery barrel.The absorbent socks were replaced in <br /> RW-4 12.77 12.82 0.05 61.70 RW-2 and RW-3.Approximately 23.75 gallons in product recovery barrel. <br /> ' RW-2 13.85 14.34 0.49 19.95 Skimmer pump in RW-4 set on continuous mode for 24 minutes;pump cycle then reset to <br /> (1)5-minute cycle/day.Approximately 11.75 gallons of product recovered from RW-4. <br /> Absorbent socks in RW-2 and RW-3 removed and strained;a negligible amount of <br /> 77/03 RW-3 13.63 15.05 1.42 5.05 product recovered.Approximately 0.25 gallons and 1.25 gallons of free product were <br /> bailed from RW-2 and RW-3,respectively,and added to the product recovery barrel.The <br /> ' absorbent socks were replaced in RW-2 and RW-3.Approximately 37 gallons in product <br /> RW-4 13.05 15.32 227 73.45 recovery barrel. <br /> Product recovery barrel measurement indicated approximately 46.75 gallons ofpmduct. <br /> RW-2 14.29 14.87 0.56 19.95 <br /> ' Full tank removed and replaced with an empty recovery barrel;skimmer pump set to <br /> continuous mode.Full product barrel set next to diesel AST basin.Skimmer pump in RW- <br /> 8/8/03 RW-3 14.23 14.94 0.71 5.05 4 set on continuous until no product recovered;pump cycle then reset to(1)10-minute <br /> cycle/day.Approximately 10.25 gallons ofpmduct recovered from RW4.Absorbent <br /> socks in RW-2 and RW-3 removed and stained;a negligible amount ofproducl <br /> ' RW-4 13.58 15.61 2.03 83.70 recovered.The absorbent socks were replaced in RW-2 and RW-3.Approximately 0.5 <br /> gallons in product recovery barrel. <br /> RW-1 13.88 13.90 0.02 Skimmer pump limed off;left in place on RW-4.Groundwater measurements in the <br /> ' RW-2 14.46 15.14 0.68 19.95 recovery wells indicated that the water level was insufficient to support skimming.The <br /> 8119/03 RW-3 NA 14.39 NA 5.05 product layer in all recovery wells was insufficient for bailing to be effective.The <br /> RW-4 NA 13.47 NA 83.70 skimmer was deactivated pending further groundwater elevation evaluation. <br /> RW-6 11 14.30 14.51 0.21 <br /> RW-1 14.01 14.03 0.02 <br /> ' RW-2 14.54 15.27 0.73 19.95 Skimmer pump deactivated and left in place in RW-4.Groundwater level in wells <br /> RW-3 14.51 15.07 0.56 5.05 insufficient to support skimming o eations.Product layer insufficient far bailing to be <br /> 829/03 RW-4 83.70 ova 6 P Y g <br /> effective.All recovery wells close to dry. <br /> RW-5 - 17.95 - <br /> ' RW-6 14.42 14.45 0.03 <br /> RW4 14.07 14.08 0.01 <br /> RW-2 14.56 15.65 0.09 19.95 Product recovery barrel measurement indicated approximately 3 gallons ofproducl. <br /> 9,5,03 RW-3 14.55 15.01 0.46 5.05 Skimmer pump amain deactivated and in place in RW-4.Groundwater level in wells <br /> RW-4 13.91 15.56 1.65 83.70 insufficient to support skimming operation.Product layer insufficient for bailing to be <br /> ' RW-5 - 14.00 - effective.All recovery wells close to dry. <br /> RW-6 14.40 14.66 0.26 <br /> RW-1 14.04 14.05 0.01 <br /> RW-2 14.61 14.65 0.04 19.95 Skimmer pump remains deactivated and in place in RW-4.Groundwater level in wells <br /> RW-3 14.62 14.85 0.23 5.05 <br /> ' 9/19/03 insufficient to support skimming operations.Product layer insufficient for bailing to be <br /> RW-4 14.00 15.20 120 83.70 effective. <br /> RW-5 14.50 <br /> RW-6 14.50 14.51 1 0.01 <br /> Skimmer pump deactivated and left in place in RW-4.Due to low gmundwater elevations being insufficient to support skimming operation,no monitoring occurred between <br /> ' Sc comber 19,2003.and December 8.2003. <br /> 1 <br /> tX:\Prcjecflaoo-pdk1838 PLOF Diesel Limol838RRep nls\1014\Ta1b1e B.xls Page 5 of 30 <br />
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