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' July 12, 1989 - UST removed along with about 25 CY spoil . Strong <br /> gasoline odor noted , and discolored soil observed at west end of <br /> tank near pump island. Three (3) soil samples tal-en; one at each <br />' end of the tanV and one about 2 ' below the tangy. . Samples delivered <br /> to Canonie labs under Chain-of-Custody. Spoil was returned to hale. <br /> July 31 , 1989 -- Sample analysis completed; see Table 1 for results. <br /> IJanuary 19-23, 1990 - Site re-entered , existing spoil removed , and <br /> an estimated 300 CY of additional spoil was removed , which resulted <br />' in a pit approximately 30 ' long X 19 ' wide X 21 ' deep. A total of <br /> seven (7) samples were collected , (see Plates IX & X , ) and were <br /> transported under Chain-of-Custody to FGL Environmental Laboratory <br />' for analysis. The spoil was placed on plastic on an asphalt storage <br /> area, and covered with plastic. <br /> February 12, 1990 -- FGL Environmental issued laboratory analysis of - <br /> Ithe above samples; refer to Table II for test results. <br /> The results of the lab tests showed that the two bottom samples <br /> showed very manor amounts of BTX&E, and no detectable levels of <br /> TPH-G, EDB, or organic lead. The sidewall samples on the northeast , <br /> east , and southeast portions of the pit were clean . The two <br /> sidewall samples on the northwest and Southwest end of the <br /> e.tcavation revealed low levels of Toluene , Xylene, and Ethyl <br /> Dibromide. Only the sample on the southwest side of the pat , <br /> (SW-2W, ) showed detectable levels of TPH-G. <br /> June 20, 1990 - Correspondence from EHD requiring a work plan for <br /> borings and/or groundwater monitoring wells. <br />' In order to define the extent and configuration of the plume, we are <br /> submitting the following Workplan for your review. Work will <br /> commence as soon as approval is received from your office. <br /> PROPOSED WORKPLAN: <br /> I1 . Drill five (5) 4" auger holes to a marc i mum depth of 40 ' at the <br /> approximate locations shown on the attached Exhibit A. If it is <br /> logistically feasible, boring No. 8-2 will be Started from the <br /> bottom of the existing excavation. If that is not possible, it will <br /> be located as close to the side of the pit as possible. <br /> 2. Split--spoon soil samples will be taken at 1 ' & 5 ' , and every 5 ' <br /> to and including the bottom of the each boring. The lithology will <br /> be described , and samples taken rind/or- supervised by a Registered <br /> Geologist. Upon completion of this phase of the word. , all borings <br />