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i <br /> The presence of diesel contamination in MW-2 indicates that diesel contamination is still <br /> affecting groundwater quality <br /> I <br /> The reversal of trends over the past 3 years may have resulted from the extreme changes in <br /> groundwater elevation,this is illustrated in Figure 9 <br /> i <br /> 6.2 Data Anomalies <br /> No data anomalies were found during this quarter's sampling <br /> 6 3 Variations from Sampling Procedures <br /> Field testing for natural attenuation indicators of groundwater samples, including pH, <br /> conductivity,and temperature,was conducted this quarter <br /> 64 Well Conditions and Appearance of Purged Water <br /> 6 4 1 MW-1 <br /> Water purged from MW-1 was dark grey in color The seal at grade was replaced in September <br /> 2005 <br /> 642 MW-2 <br /> . The water purged from MW-2 has visible floating product but is otherwise clear The seal at <br /> grade and the well cap are deteriorating <br /> 6 4 3 MW-3 <br /> MW-3's purged water is clear and free from any floating product <br /> 644 MW-4 <br /> Water purged from MW4 is silty with a slight hydrocarbon odor The well is in good <br /> condition <br /> 6 5 Management of Purge Water <br /> Water purged from MW-1,MW-3 and MW-4 as well as decontamination water was placed in a <br /> 55-gallon drum and removed from the site by Douios Environmental,Inc <br /> I <br /> 6 6 Recommendations <br /> EI recommends <br /> ■ Continued removal of floating oil from MW-2 every quarter until motor oils no longer <br /> appear <br /> • Continued quarterly monitoring of the four groundwater monitoring wells at CTL to <br /> i <br /> 7160 <br /> I <br />