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ARCHIVED REPORTS XR0009370
EnvironmentalHealth
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EHD Program Facility Records by Street Name
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EL DORADO
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3105
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2900 - Site Mitigation Program
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PR0542208
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ARCHIVED REPORTS XR0009370
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Entry Properties
Last modified
7/24/2019 5:00:07 PM
Creation date
7/24/2019 4:48:14 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0009370
RECORD_ID
PR0542208
PE
2960
FACILITY_ID
FA0024243
FACILITY_NAME
CALIFORNIA TANK LINES
STREET_NUMBER
3105
Direction
S
STREET_NAME
EL DORADO
STREET_TYPE
ST
City
STOCKTON
Zip
95206
APN
17512028
CURRENT_STATUS
01
SITE_LOCATION
3105 S EL DORADO ST
P_LOCATION
01
QC Status
Approved
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SJGOV\wng
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EHD - Public
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1 <br /> The reversal of trends over the past 3 years may have resulted from the extreme changes in <br /> groundwater elevation,this is illustrated in Figure 9 <br /> 6.2 Data Anomalies <br /> No data anomalies were found during this quarter's sampling <br /> 6.3 Variations from Sampling Procedures <br /> iField testing for natural attenuation indicators of groundwater samples, including pK <br /> conductivity,and temperature,was conducted this quarter <br /> 6.4 Well Conditions and Appearance of Purged Water <br /> ' 6 4.1 MW-1 <br /> Water purged from MW-1 has a slight hydrocarbon odor The seal at grade has been <br /> deteriorating since installation due to the large number of trucks that pass over it daily Also, <br /> t the well cap needs replacement <br /> 6 4.2 MW-2 <br /> rThe water purged from MW-2 has visible floating product but is otherwise clear As with MW- <br /> 1,the seal at grade and the well cap are deteriorating <br /> 6.4.3 MW-3 <br /> MW-3's purged water is cloudy and free from any floating product The well cap needs <br /> 1 replacement <br /> 6 4 4 MW-4 <br /> ' Water purged from MW4 is silty with a slight hydrocarbon odor The well is in good <br /> condition <br /> 6.5 Management of Purge Water <br /> Water purged from MW-i, MW-3 and MW4 as well as decontamination water was placed in <br /> ' e an on-site 55-gallon drum and labeled <br /> E <br /> 6.6 Recommendations <br /> El recommends <br /> ■ Continued removal of floating oil from MW-2 every four weeks until motor oils no <br /> longer appear <br /> ■ Continued quarterly monitoring of the four groundwater monitoring wells at CTL to <br /> accumulate data as a basis for future actions, or to show when contamination levels <br /> have dropped to insignificant levels <br /> L r_ 5 <br />
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