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ARCHIVED REPORTS XR0009950
EnvironmentalHealth
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EHD Program Facility Records by Street Name
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EL DORADO
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7906
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2900 - Site Mitigation Program
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PR0540858
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ARCHIVED REPORTS XR0009950
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Last modified
8/1/2019 11:51:56 AM
Creation date
8/1/2019 10:52:37 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0009950
RECORD_ID
PR0540858
PE
2960
FACILITY_ID
FA0023360
FACILITY_NAME
ARCO SERVICE STATION #2130
STREET_NUMBER
7906
Direction
N
STREET_NAME
EL DORADO
STREET_TYPE
ST
City
STOCKTON
Zip
95210
CURRENT_STATUS
01
SITE_LOCATION
7906 N EL DORADO ST
QC Status
Approved
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EHD - Public
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• Mr Kyle Christie Project 0805-114 04 <br /> May 15, 1995 <br /> Page 4 <br /> 70 cubic/feet per irunute, the amount of gasoline removed through the end o the first <br /> quarter 1995 is estimated to be approximately 11,007 pounds or 1,784 gallons <br /> Soil vapor extraction wells VW-1 through VW-12 were all fully opened since start-up until <br /> January 3, 1995 Since then, the system has been operating ith VW-5, VW-9, VW-11, <br /> and VW-12 closed (see Table 5) The air sparge system was shut down on February 3, <br /> 1995, along with the rest of the system. <br /> The remediation %ystem was shut off on February 3, 1995 after sample results from <br /> January 23, 1995, showed poor removal rate (approximately 27 percent),by the catalytic <br /> oxidizer The unit remained off throu h the end The catalyst was removed <br /> and analyzed by AIREX Early analysis indicated that the catal%st had been exposed to high <br /> temperatures outside operational parameters and failed The failure is calledcatai st <br /> centerin AIREX is currently reviewing the control system and other equipment to <br /> prevent any future problems <br /> ACTIVITIES PERFORMED DURING THE FIRST QUARTER <br /> A ; ue:�1n-rereent was mailed to Mr and Mrs Cheam cproperty owners north of the <br /> onJan5, 1995 <br /> ANTICIPATED WORK <br /> Once ARCO has received authorization to drill on the adjacent property north of the site, a <br /> workplan outhr ung additional assessment activities will be submitted to the SJCPHS as well as <br /> the necessary permit application <br /> ARCO will continue to perform quarterly groundwater monitoring The next sampling <br /> event is scheduled in May 1995 <br /> CONCLUSIONS <br /> Hydrocarbon concentrations continue to fluctuate in groundwater underlying the site The <br /> st c ncentxations were detected iii wells MW-1 and MW-5 The groundwater flow <br /> direction was towards the east, which is generally consistent with past data EMCON requests <br /> the assistance from the SJCPHS to obtain access from the adjacent property owners to the <br /> liorth <br /> W NN pio'sp8OW8051140 4bs-95 pas 5 <br />
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