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ARCHIVED REPORTS XR0009962
EnvironmentalHealth
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EHD Program Facility Records by Street Name
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EL DORADO
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7906
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2900 - Site Mitigation Program
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PR0540858
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ARCHIVED REPORTS XR0009962
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Last modified
8/1/2019 12:22:48 PM
Creation date
8/1/2019 10:57:43 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0009962
RECORD_ID
PR0540858
PE
2960
FACILITY_ID
FA0023360
FACILITY_NAME
ARCO SERVICE STATION #2130
STREET_NUMBER
7906
Direction
N
STREET_NAME
EL DORADO
STREET_TYPE
ST
City
STOCKTON
Zip
95210
CURRENT_STATUS
01
SITE_LOCATION
7906 N EL DORADO ST
QC Status
Approved
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EHD - Public
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DISCUSSION <br /> • Results of this monitoring event indicate that concentrations of dissolved gasoline hydrocarbons in wells <br /> MW-1 through MW-7 and MW-10 are generally consistent with results from previous sampling events <br /> The highest levels of TPHG and benzene, were detected in MW-2 at concentrations of 435 µg/l and 33 <br /> pg/I, respectively As in previous quarters, no constituents were detected in wells MW-3, MW-4, and <br /> MW-7 <br /> Oxygenates, TBA, MTBE, DIPS, ETBE, and TAME were analyzed in samples collected from groundwater <br /> monitoring wells MW-1 through MW-7, and MW-10 using USEPA Method 8260 MTBE was detected only <br /> in MW-2 at a concentrations of 6 3 µg11, within the range of previous sampling results MTBE was not <br /> detected in MW-5 after being detected the previous eight quarters No other oxygenates were detected in <br /> the wells <br /> The groundwater gradient (0 0015) and direction of groundwater flow (east-northeast) were generally <br /> consistent with previous data Groundwater elevation decreased an average of approximately 2 56 feet <br /> from the previous sampling event(March 2000) <br /> The soil vapor extraction system has not been operational since November 1987 Inspection of the <br /> system in June, 2000 indicates that the heating coil needs replacement <br /> ATTACHMENTS <br /> • Table 1 Groundwater Monitoring Data <br /> • Table 2 Groundwater Analytical Results for Oxygenates <br /> • Table 3 Operational Uptime Information of the Soil Vapor Extraction System <br /> • Table 4 Flow Rates and Results of Air Sample Analyses <br /> . • Table 5 Extraction and Emission Rates <br /> • Table 6 Air Sparge and Air Bubbling Flow Rates and Dissolved Oxygen Levels <br /> • Figure 1 Site Location Map <br /> • Figure 2 Groundwater Elevation Contours (Second Quarter 2000) <br /> • Figure 3 Groundwater Analytical Summary (Second Quarter 2000) <br /> • Appendix A Sampling and Analysis Procedures <br /> • Appendix B Chain-of-Custody Records and Laboratory Analysis Records <br /> • Appendix C Operation and Maintenance and Groundwater Monitoring Field Data Sheets <br /> C IARC0121301QT'RLY1200012130g200 doe Delta <br /> 09/19/00 <br />
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