Laserfiche WebLink
CURRENT SOURCE (BEFORE DILUTION) INFLUENT SUMMARY (LAB) <br /> Total Petroleum Hydrocarbons as <br /> Gasoline (TPHG) Conc This Period SVE system down since 11/24/97 due to low TPHG <br /> concentrations in soil vapor <br /> TPHG Conc Last Period NA <br /> Initial TPHG Conc 9,900 mg/m3 (November 9, 1994 [following system upgrade]) <br /> Benzene Conc This Period NA <br /> Benzene Conc Last Period NA <br /> Initial Benzene Concentration 290 mg/m3 (November 9, 1994[following system upgrade]) <br /> DISCUSSION <br /> Results of this monitoring event indicate that concentrations of dissolved gasoline hydrocarbons in wells <br /> MW-1 through MW-7, and MW-10 are consistent with levels detected in previous sampling events, with <br /> the following exceptions Well MW-3 contained a TPHG concentration of 71 6 micrograms per liter (µgfl, <br /> and well MW-5 contained an MTBE concentration of 5 15 µg/L The groundwater gradient and direction of <br /> groundwater flow (east-southeast) were also generally consistent with previous data Groundwater <br /> elevation decreased approximately 1 76 feet from the previous sampling event (June 1998) <br /> The oxygenates, tertiary butanol, MTBE, di-isopropyl ether, ethyl tertiary butyl ether, and tertiary amyl <br /> methyl ether were analyzed for wells MW-1 through MW-7, and MW-10 using USEPA Method 8260 No <br /> oxygenates were detected in the samples from wells MW-1, MW-2, MW-3, MW-4, MW-6, MW-7, and MW- <br /> 10 (see Table 2) Due to non-detect analytical results for oxygenates (other than MTBE,) using <br /> USEPA 8260 for all wells, Pinnacle, on behalf of ARCO, requests no further analysts for oxygenates with <br /> the exception of MTBE using only USEPA Method 8020 <br /> Pinnacle shut down the SVE system on November 24, 1997, due to low sod vapor concentrations and is <br /> currently pulsing the system on a periodic basis (one week per month, if warranted) The SVE system <br /> remained shut down during the third quarter 1998 <br /> The air sparge system was shut down on November 24, 1997, along with the SVE system to evaluate <br /> feasible remediation alternatives Based on data and remediation techniques evaluation, the air sparge <br /> system was restarted on January 20, 1998, and operated at a low flow rate for bubbling and oxygen <br /> addition to the groundwater The addition of oxygen into the groundwater will help to promote <br /> biodegradation of petroleum hydrocarbons in impacted groundwater at the site As a result of air bubbling <br /> in air sparge wells AS-1, AS-2, and AS-3, since January 1998, dissolved oxygen levels in monitoring wells <br /> MS-1(s), MS-2(s), MS-3(s), and MW-2 have increased significantly as shown in Table 3 Pinnacle will <br /> continue to monitor the effects of SVE system pulsing and air bubbling during the fourth quarter 1998 <br /> ATTACHMENTS <br /> • Table 1 Groundwater Monitoring Data <br /> • Table 2 Groundwater Analytical Results for Oxygenates <br /> • Table 3 Air Sparge/Air Bubbling Flow Rates and Dissolved Oxygen Levels <br /> • Figure 1 Site Location Map <br /> • Figure 2 Groundwater Analytical Summary (Third Quarter 1998) <br /> • Figure 3 Groundwater Contour Elevations (Third Quarter 1998) <br /> • Appendix A Sampling and Analysis Procedures <br /> Cp1D 1QMR13RDQTR-112130Q398 DOC-98Vsg 1 Pce <br /> Rev 11/19/98 <br />