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ARCHIVED REPORTS_XR0008496
EnvironmentalHealth
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3500 - Local Oversight Program
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PR0545859
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ARCHIVED REPORTS_XR0008496
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Last modified
6/3/2020 5:10:28 PM
Creation date
8/15/2019 11:56:00 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0008496
RECORD_ID
PR0545859
PE
3528
FACILITY_ID
FA0003831
FACILITY_NAME
WATERLOO FOODMART
STREET_NUMBER
4315
Direction
E
STREET_NAME
WATERLOO
STREET_TYPE
RD
City
STOCKTON
Zip
95215-2305
APN
08710034
CURRENT_STATUS
02
SITE_LOCATION
4315 E WATERLOO RD
P_LOCATION
99
P_DISTRICT
004
QC Status
Approved
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EHD - Public
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CAM 13RIA <br /> EPA Method 8260B Groundwater samples from the wells were <br /> also analyzed for ethanol by EPA Method 8260B <br /> Soil Disposal Approximately 12 cubic yards of soil were generated during <br /> field activities, stored onsite, and covered with plastic sheeting <br /> The soil stockpile was sampled and profiled for disposal <br /> (laboratory data in Appendix E) On November 29, 2001, <br /> Manley and Sons Trucking, Inc of Sacramento, California <br /> transported the soil to Allied Waste Industries' Forward Landfill <br /> in Manteca, California for disposal <br /> Well Materials Wells MW-2 through MW-4 were constructed using four-inch <br /> diameter, Schedule 40 PVC casing with a screen slot size of <br /> 0 020-inch and#2/12 Monterey sand <br /> Screened Interval. Wells MW-2 through MW-4 are screened from 47 to 72 fbg <br /> Monitoring well construction details are presented on Table 1 <br /> and recorded on the exploratory boring logs (Appendix C) <br /> Well Development/Sampling Blaine developed and purged wells MW-2 through MW-4 on <br /> November 14, 2001 and sampled the site wells on <br /> November 16, 2001 Blaine developed the wells using surge <br /> block agitation and pump evacuation Blaine's groundwater <br /> monitoring and well development report, which includes field <br /> sheets, is presented as Appendix D <br /> Wellhead Survey Virgil Chavez Land Surveying (licensed land surveyor <br /> No 6323) of Vallejo, California surveyed the top of casing <br /> elevations for wells MW-1 through MW`4 relative to mean sea <br /> Ievel on December 20, 2001 (Appendix F) <br /> Groundwater Flow Direction Cambria evaluated water-level measurement data from <br /> November 16, 2001 and prepared a groundwater contour map <br /> (Figure 3) Groundwater flow direction is to the northwest this <br /> quarter at an approximate hydraulic gradient of 0 1 <br /> • <br /> 1359 5 <br />
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