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ARCHIVED REPORTS XR0006360
EnvironmentalHealth
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2900 - Site Mitigation Program
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PR0519189
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ARCHIVED REPORTS XR0006360
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Last modified
8/21/2019 4:28:25 PM
Creation date
8/21/2019 2:31:25 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0006360
RECORD_ID
PR0519189
PE
2950
FACILITY_ID
FA0014347
FACILITY_NAME
CURRENTLY VACANT
STREET_NUMBER
6425
STREET_NAME
PACIFIC
STREET_TYPE
AVE
City
STOCKTON
Zip
95207
APN
09741031
CURRENT_STATUS
02
SITE_LOCATION
6425 PACIFIC AVE
P_LOCATION
01
QC Status
Approved
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EHD - Public
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R603 UPDATE-22 11/11/93 <br /> range hydrocarbons on July 19, 1993 . With the addition of the <br /> heat exchanger the pounds per day destruction was increased to <br /> nearly 70 pounds per day on August 23, 1993 , just prior to <br /> turning the system off for repair of the compressor and changing <br /> out the pilot/burner assembly. Presently the system is <br /> destroying 30 to 40 pounds per day of gasoline range <br /> hydrocarbons, see Table 2 and concentration charts Figures 5A, <br /> 5B, 5C, 5D, 5E and 5F. These charts indicate that the heavier <br /> compounds of gasoline range hydrocarbons ethylbenzene, xylenes, <br /> etc ) have been moderately reduced while lighter compounds <br /> (benzene, toluene, etc. ) have been greatly reduced. <br /> CONDENSATE REMOVAL BY LTT <br /> Condensation from vapor extraction is collected in moisture drop <br /> out tanks constructed of 12" PVC pipe, before the manifold, to <br /> prevent moisture build up on the vacuum pump filter. All fluids <br /> removed from the condensation traps are placed in the 1000 gallon <br /> "ConVault" Table 5 represents the field notes from LTT <br /> condensate/water removal, see Appendix B. As of November 5, 1993 <br /> LTT has removed an estimated 4915 gallons of condensate/water and <br /> 26 25 gallons of product from the condensate traps . Total fluids <br /> removed as of August 30, 1993 : 5077 gallons of water/condensate <br /> and 48 . 75 gallons of product (162 previously recovered condensate <br /> water and 22 . 5 gallons of product) . <br /> 4 . 0 SUMMARY <br /> There has been no evidence of floating product or product sheen <br /> on the ground water in MW1 since April 14, 1992 and MW3 and MW10 <br /> since November 11, 1992 Only occasional product sheen is found <br /> with the condensate recovered from the vapor extraction moisture <br /> dropouts and manifold. Vapor recovery and well purging has <br /> reduced the hydrocarbons in ground water significantly since the <br /> May 25, 1990 sampling, see Table 1 . Using benzene as an <br /> indicator, monitoring wells MW4, MW5, MW6 , MW7 and MW9 have been <br /> reduced to below detection limits while the wells being utilized <br /> for vapor extraction (MW1, MW3 , and MW10) have been reduced by <br /> better than 99%s MW2 , which is also utilized for vapor <br /> extraction has been reduced 81's and MW8 has been reduced by <br /> approximately 22%s Of the newly installed wells MW11 and MW12 , <br /> MW12 has not shown any significant change in benzene <br /> U V1 .ClH.«Gt1V1s al-LA M.71"1 116.10 -1 r%QYO 1'69F46ct, on <br /> � 'e . re1A.J1 " L lm *n <br /> 11LLL 1..0 <br /> On August 23 , 1993 , a sample of the water being treated by air <br /> stripping inside the "ConVault" was obtained for certified <br /> laboratory analysis, before dumping the approximately 700 gallons <br /> of this cleaned water to the City of Stockton' s sanitary sewer, <br /> see Appendix A. <br /> As of November 5, 1993 , an estimated 21887 gallons of gasoline <br /> range hydrocarbons have been removed from the soil and ground <br /> water beneath this site . Previously removed floating product <br /> (40 25 gallons) , condensation from vapor extraction (46 75 <br /> PAGE 3 <br />
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