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ARCHIVED REPORTS XR0006534
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2900 - Site Mitigation Program
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PR0519189
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ARCHIVED REPORTS XR0006534
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Last modified
8/21/2019 4:44:14 PM
Creation date
8/21/2019 3:05:52 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0006534
RECORD_ID
PR0519189
PE
2950
FACILITY_ID
FA0014347
FACILITY_NAME
CURRENTLY VACANT
STREET_NUMBER
6425
STREET_NAME
PACIFIC
STREET_TYPE
AVE
City
STOCKTON
Zip
95207
APN
09741031
CURRENT_STATUS
02
SITE_LOCATION
6425 PACIFIC AVE
P_LOCATION
01
QC Status
Approved
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EHD - Public
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i <br /> R603 UPDATE-19 8/24/93 <br /> (ethylbenzene, xylenes, etc ) <br />• CONDENSATE REMOVAL AND WELL PURGING BY LTT <br /> Condensation from vapor extraction is collected in moisture drop <br /> out tanks constructed of 12 " PVC pipe, before the manifold, to <br /> prevent moisture build up on the vacuum pump filter All fluids <br /> removed from the condensation traps are placed in the 1000 gallon <br /> "ConVault" Table 5 represents the field notes from LTT <br /> condensate removal and well purging (MW2 and MW3 condensate into <br /> the same trap and the condensate removal is represented with MW2 <br /> data) , see Appendix B. As of July 27, 1993 LTT has removed an <br /> estimated 4602 gallons of ground water from MW1, MW2, MW3, MW8, <br /> MW10 and water condensate from traps for MW2&3 , MW10, EX and <br /> 26 25 gallons of product from the condensate traps Total fluids <br /> removed as of July 27, 1993 4764 gallons of ground <br /> water/condensate water and 48 . 75 gallons of product (162 <br /> previously recovered condensate water and 22 5 gallons of <br /> product) <br /> 4 . 0 SUMMARY <br /> There has been no evidence of floating product or product sheen <br /> on the ground water in MW1 since April 14, 1992 and MW3 and MW10 <br /> since November 11, 1992 Only occasional product sheen is found <br /> with the condensate recovered from the vapor extraction moisture <br />• dropouts and manifold Vapor recovery and well purging has <br /> reduced the hydrocarbons in ground water significantly since the <br /> May 25, 1990 sampling, see Table 1 . Using benzene as an <br /> indicator, monitoring wells MW4 , MWS, MW6, MW7 and MW9 have been <br /> reduced to below detection limits while the wells being utilized <br /> for vapor extraction (MW1, MW3 , and MW10) have been reduced by <br /> better than 9911 MW2, which is also utilized for vapor <br /> extraction has been reduced 81s and MW8 has been reduced by <br /> approximately 22% Of the newly installed wells MW11 and MW12, <br /> MW11 has always tested below detection limits MW12 has not <br /> shown any significant change in benzene concentrations <br /> On June 14 , 1993 , a sample of the water being treated by air <br /> stripping inside the "ConVault" was obtained for certified <br /> laboratory analysis, before dumping approximately 800 gallons of <br /> this water to the City of Stockton' s sanitary sewer, see Appendix <br /> A <br /> As of June 22 , 1993 , an estimated 21432 gallons of gasoline range <br /> hydrocarbons have been removed from the soil and ground water <br /> beneath this site. Previously removed floating product (40 .25 <br /> gallons) , condensation from vapor extraction (48 75 gallons) , <br /> Projected petroleum hydrocarbon in situ oxidation CO2 vapor <br /> recovery (63240 pounds/6 25 pounds/gallon = 1017.8 gallons) and <br /> vapor extraction-destruction of hydrocarbons (70155 pounds/6 25 <br /> 11225 gallons) . No chlorinated solvents were detected in <br /> chromatogram comparisons, 113. e . « 1, 2, -Dichloroethane (DCE) <br /> . retention time 2 . 079 minutes, Trichloroethylene (TCE) - retention <br /> PAGE 3 <br />
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