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L SUBMIT IN DUPLICATE <br /> RESOURCES AGENCY OF CALIFORNIA <br /> DEPARTMENT OF CONSERVATION OF OIL API, <br /> L DIVISION OF OIL AND GS -; ECEIVED <br /> History of Oil or Gas well 1 JUL 2 61988 <br /> L 'OODLAND, CALIFORNIA <br /> Operator.....QRI.QN. .QI.L..CQMPAN.Y.,OF CA.... Field ........-.--.1............. Count SAN JOAQUIN <br /> L <br /> Well...........ARNAUQO...QR.QS ��1............_... ...... .. .... ......... . Sec._5.�... T....25.., R .- E...,M... B. & M. <br /> A.P.I. No... 7. -.205.IQ...............y........ Name........M.I.CHAEL... ...__BUNYbK_....: Tit1e.......DRLG SUPT <br /> Date ....... ...,2- :...... , I9 J7. (hn.nwbmiui.Er.p.r" LPreide.[,s .R`«A.,.eo <br /> L Signattfre�?.�! '�e "ZI7 / <br /> — <br /> ..3.2.Q,1...5KYWAY...DRI.YE...STE.. 104, SANTA MARIA , CA 934 5 805-922-0376 <br /> ....... <br /> LAddrea[, . tTaNpY.ae Rwnbcr) <br /> History must be complete in all detail. Use this form to report an o <br /> or altering the casing,plugging, at Aerations during drilling and listing o the well test <br /> duringg ramou ng <br /> g g,p gging,or abandonment with the dates thereof.Include such items as hole size,formation fes[details,amounts <br /> of cement used, top and bottom of plugs,perforation details, sidetracked junk, bailing 6�x and initiaj production data. <br /> Ds[e <br /> CONDITION OF HOLE IN START : CONDITION OF HOLE @ COMPLETION : <br /> NEW WELL TD : 3700 ' ET 2970 ' KB : 10 ' <br /> .. 16" C 50 ' <br /> 1.0-3/4" C 960 ' <br /> 7" 2346 K-55 C. 2]]90 ' <br /> 5-1/2" 1741: K-55 SFJ C 2387 ' -3104 ' <br /> PERFS 2830 ' -20371 , 2844 ' -2846 ' <br /> 2-3/8" 4 . 7# W/311 0. 12 SSWW L 27321 - <br /> 2856 ' <br /> r <br /> FISH 3540' -3556' <br /> CMT PLUG : 31891' -3343 ' <br /> L DAY <br /> 'ENDS 12 :00 <br /> MIONI HT <br /> L <br /> 1988 DEPTH DESCRIPTION <br /> 4-15 50 ' - MIRU GARY RIG #9 W/10' KB. SPUD @' 1 OO HRS. ' WELD ON <br /> 197 ' STARTING FLANGE ON 16" CONDUCTOR . N 16" HYDRIL 3M (6") <br /> DIVERTER LINE . MU BHA #1 . FUNCTION TSTD DIVERTER SYSTEM . <br /> LSPUD THRU 16" COND @ 2000 HRS . DRLD 14-3/4" HOLE 50 ' -197 ' . <br /> MUD : 65 PCF ; . 451 PSI/FT GRAD ; 45 FUN VIS . <br /> 4-16 197 ' - DRLD 197 ' -270 ' . CIRC OUT MUD RING. TRIPPED TO CLEAN BIT <br /> L 960 ' & STAB. (BALLED UP) . DRLD & SUR 270 ' -9601 . CIRC CLEAN . <br /> WIPER TRIP TO 14-3/4" STAB . RMD 9301' -960 ' , CO MUD RING. <br /> POOH W/BHA 41.1 FOR LOGS . RU SCHLUMBE�tGER W/LUBRICATOR. RAN <br /> '` DIL/SFL/GR. WKD THRU TIGHT SPOT @ 4111 ' . UNABLE TO PASS <br /> 678 ' . LOGGED 673 ' -50 ' RD SCHLUMBEPGER . MU BHA 411 . RAN <br /> TO 960 ' . CIRC CLEAN . POOH FOR 10-3/4" CSG . RU & RNG CSG. <br /> MUD : 65 PCF; .451 PSI/FT GRAD ; 45 F N VIS . <br /> L <br /> L <br /> OG103 f5/e5/OWRR/5MI <br />