My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
SU0002188_SSNL
EnvironmentalHealth
>
EHD Program Facility Records by Street Name
>
E
>
88 (STATE ROUTE 88)
>
13731
>
2600 - Land Use Program
>
UP-99-21
>
SU0002188_SSNL
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
11/20/2024 9:21:58 AM
Creation date
9/4/2019 6:11:53 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2600 - Land Use Program
FileName_PostFix
SSNL
RECORD_ID
SU0002188
PE
2626
FACILITY_NAME
UP-99-21
STREET_NUMBER
13731
Direction
N
STREET_NAME
STATE ROUTE 88
City
LODI
Zip
95240
ENTERED_DATE
10/23/2001 12:00:00 AM
SITE_LOCATION
13731 N HWY 88
QC Status
Approved
Scanner
SJGOV\rtan
Supplemental fields
FilePath
\MIGRATIONS\E\HWY 88\13731\UP-99-21\SU0002188\NL STDY.PDF
Tags
EHD - Public
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
63
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
r. .o 1 Its NEIL O.-ANDERSON &ASSOCIATES, INC. <br /> ' O,y GEOTECHNICAL•ENVIRONMENTAL•INSPECTIONS•TESTING•LABORATORY SERVICES <br /> SACRAMENTO OFFICE CORPORATE OFFICE <br /> � v x '4229 Northgate Boulevard,Suite 3 22 Houston Lane <br /> p Crnco (530)s91-6104 Sacramento,California 95834 Lodi,California 95240 <br /> P srocccraN;(zo9)47x.iovi (916)929-9267, (209)367-3701 <br /> °s S O c\ kAT. fiocoxnovA X916)631-4455 FAX:(916)929-9269 „FAX:(209),333-8303 <br /> November 8, 2001 <br /> Mike Smith <br /> Mike Smith Engineering ... <br /> 4 N. Main St..' <br /> k..: Lodi, CA 95240 i <br /> MOWED <br /> Subject:' Engineered Septic Systems <br /> Omega Vineyard, Phase I ;r. $.EP 0.5. 2002 <br /> 13731 N Hwy-88 at:Harney Ln. <br /> ENVIRONMENT HEALTH <br /> Lodi, California <br /> PERMIT/SERVICES <br /> Our Job Number: LG00-287 <br /> 'Dear Mike: ; <br /> Our office performed a soil suitability/nitrate loading study for the subject project and the <br /> --results are contained'in our report.dated October 4,'2001. In the report we concluded that dile to <br /> the presence of clayey soils;'an engineered septic system would be required. This letter presents <br /> a summary of our engineering and subsequent recommended septic system design.. <br /> L Background4nd Proposal <br /> 'After conversations-with Mike,Smith Engineering and,the results of our numerous.test <br /> borings and percolation WAS performed on the site, it was decided that-the:most favorable <br /> location for a septic disposal-field was:the northeast corner of the site. Subsequently, two <br /> shallow and one deep percolation tests.were performed in this location. The lbcation and results <br /> of these tests are contained'in our Oct. 4 report. `The deep pit test,was performed using,an <br /> alternate-method where the full depth of the-test;hole(25' deep) is percolated.and a clear water <br /> rate.is determined. <br /> An estimated design flow for the proposed new system is shown in the following Table 1: <br /> Table I Estimated Daily Effluent Flow <br /> Category Effluent usage for each People per day Effluent quantity per category <br /> category <br /> Employees 15 gals 10 10 people x 15 gal/person-day= 150 gallday <br /> Customers . 10'gals 20 20 people x 10 gal/person-day=.200 gal/day <br /> Daily Flow: 350 gals/day.. <br />
The URL can be used to link to this page
Your browser does not support the video tag.