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i ! <br /> . Groundwater Elevation Data <br /> Depth to groundwater was obtained from the existing groundwater monitor wells at the site using a <br /> water level indicator graduated to 0 01 foot The depth to groundwater measurement was converted <br /> to a groundwater elevation for each well and used to construct a groundwater elevation contour map <br /> (Figure 2), and calculate the local groundwater flow direction and hydraulic gradient Groundwater <br /> at the site was measured at depths between 68 90 to 76 94 feet below ground surface (bgs) The <br /> groundwater potentiometric surface elevation averaged approximately 26 85 feet bgs during this <br /> monitoring event The groundwater elevation has decreased approximately 145 feet since the last <br /> sampling event in April 2001 The groundwater flow direction during this reporting period is toward <br /> the southwest with a hydraulic gradient of approximately 0 02 ft/ft A summary of data regarding <br /> groundwater levels measured through August 20, 2001 is presented in Table 1 Copies of field <br /> observations documenting work performed at the site are presented in Attachment I <br /> Groundwater Analytical Results <br /> The distribution of groundwater sample analytical results obtained from monitor wells at the site on <br /> August 20,2001,is presented on Figure 3 and summarized in Table 2 Due to the presence of liquid <br /> phase hydrocarbon (LPH),the highest concentration of petroleum hydrocarbons is in the vicinity of <br /> monitor well MW-1 TPHg and benzene concentrations were below method detection limits for all <br /> wells sampled during this monitoring event MTBE concentrations were below method detection <br /> limits for all wells sampled except MW-4 (1 1 ug/1) during this monitoring event Attachment H <br /> contains photocopies of the laboratory analytical report and the chain-of-custody form <br /> iApproximately 0 52 feet of LPH was detected in MW-1 during this monitoring event The LPH is <br /> currently being removed from MW-1 by hand bailing methods and the use of a passive, down-hole <br /> petroleum skimmer on a weekly basis The LPH thickness has generally decreased in MW-1 since it <br /> was first observed in February 2000 A total of approximately 55 gallons of LPH has been removed <br /> from MW-1 since its detection in February 2000 <br /> Purge Water <br /> Purge water generated dunng groundwater purging is currently contained on-site in Department of <br /> Transportation rated 55-gallon drums and will be removed to a disposal/recycling facility during <br /> November 2001 <br /> SITE REMEDIATION <br /> Construction of a soil and groundwater remediation system was completed at the site in December <br /> 1999 The remediation system consists of seven soil vapor extraction (SVE) wells (W-1, W-3 <br /> through W-8), two groundwater monitor wells modified for SVE (MW-1 and MW-3) and four air <br /> sparge wells (AS-1 through AS-4) with catalytic oxidation treatment A Site Plan depicting the <br /> locations of the remediation wells, subsurface piping, and remediation equipment compound is <br /> included as Figure 4 Initial start-up air discharge compliance testing was completed on December <br /> 13, 1999 The San Joaquin County Valley Air Pollution Control District(SJVAPCD)has approved <br /> an air permit for the site During site visits, SECOR monitored system parameters and collected <br /> C 171me OiN.ockefordQ301 <br /> 2 SECOR <br /> 077 41737 003 November 8,2001 <br />