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ARCHIVED REPORTS_XR0007165
EnvironmentalHealth
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3500 - Local Oversight Program
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PR0544811
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ARCHIVED REPORTS_XR0007165
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Last modified
11/20/2024 9:21:19 AM
Creation date
9/5/2019 1:48:08 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0007165
RECORD_ID
PR0544811
PE
3528
FACILITY_ID
FA0000091
FACILITY_NAME
Colonial Energy CE 40138 (DBA Power Mart)
STREET_NUMBER
14000
Direction
E
STREET_NAME
STATE ROUTE 88
City
LOCKEFORD
Zip
95237
CURRENT_STATUS
02
SITE_LOCATION
14000 E HWY 88
P_LOCATION
99
P_DISTRICT
004
QC Status
Approved
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EHD - Public
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collected from MW-4, MW-7, MW-8, MW-9 or MW-10 No sample was submitted from MW-1 due to the <br /> presence of free product Table 2 and Table 3 in the attached report summarize groundwater analytical data <br /> and laboratory reports are included as Attachment 2 <br /> The highest concentrations of hydrocarbons appear to remain onsite in the vicinity of the pump islands (MW- <br /> 1) <br /> MW1) and somewhat downgradient of the tank system When compared to the August 2000 sampling event, <br /> hydrocarbon concentrations increased slightly in MW-4 and MW-5, while they decreased slightly in MW-3 <br /> Hydrocarbon concentrations remained relatively unchanged in the remainder of the wells Changes in <br /> hydrocarbon concentrations are most likely a result of groundwater elevation fluctuations and remediation <br /> efforts Since the initiation of remediation efforts, hydrocarbon concentrations across the site have generally <br /> decreased <br /> The appearance of free product in MW-1 appears to be the result of condensed sod vapor due to vapor <br /> extraction efforts Site inventory records and leak detection systems were checked to assure that a new <br /> release had not occurred, no indications of a release were identified At this time product is being removed <br /> from MW-1 by hand bailing and the use of a passive skimmer in addition to continued vapor extraction <br /> efforts <br /> Remediation Activities—Fourth Quarter 2000 <br /> In August and September 1999, SECOR installed a vapor extraction/air sparging system at the subject site to <br /> remediate hydrocarbon-impacted soils and groundwater System operation began December 13, 1999 <br /> The vapor extraction system consists of ten wells (W-1 through W-8, MW-1 and MW-3) manifolded within the <br /> remediation compound Vapors are extracted with a blower and destroyed with a catalytic oxidizer with a <br /> destruction efficiency of at least 95% The air sparging system consists of 4 wells (AS-1 through AS-1) An <br /> air compressor is used to introduce air into the sparging wells, and recovered vapors are destroyed with the <br /> SVE system <br /> Based on the analysis of influent samples, SECOR estimates that 2,979 pounds (488 4 gallons) of gasoline <br /> were removed and treated during the reporting period at an average extraction rate of 187 scfm SECOR <br /> estimates that 29,680 9 pounds (4,865 7 gallons) of hydrocarbons have been removed since system startup <br /> Approximately 40 gallons of free product have been bailed from MWA since its detection if February 2000 <br /> Attachment 3 in SECOR's report includes soil vapor analytical results and system efficiency results <br /> If you have any questions regarding these matters, please do not hesitate to contact me at(206) 286-4495 <br /> Sincerely, <br /> Time Oil Co <br /> Anastasia E Duarte-Wilkinson <br /> Environmental Toxicologist <br /> cc Ms Elizabeth Thayer <br /> California Regional Water Quality Control Board <br /> i <br /> 2 <br />
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