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SU0006227 SSCRPT
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SU0006227 SSCRPT
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Last modified
12/17/2019 11:37:58 AM
Creation date
9/6/2019 10:17:52 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2600 - Land Use Program
FileName_PostFix
SSCRPT
RECORD_ID
SU0006227
PE
2620
FACILITY_NAME
PA-0600127
STREET_NUMBER
22261
Direction
S
STREET_NAME
MOUNTAIN HOUSE
STREET_TYPE
PKWY
City
MOUNTAIN HOUSE
ENTERED_DATE
8/29/2006 12:00:00 AM
SITE_LOCATION
22261 S MOUNTAIN HOUSE PKWY
RECEIVED_DATE
8/28/2006 12:00:00 AM
P_LOCATION
99
P_DISTRICT
005
QC Status
Approved
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SJGOV\sballwahn
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FilePath
\MIGRATIONS\M\MOUNTAIN HOUSE PKWY\22261\PA-0600127\SU0006227\SSC RPT.PDF
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EHD - Public
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r kN1 KLEINFELDER <br /> s� 1 EXECUTIVE SUMMARY <br /> According to Chevron Pipeline Company, an 18-inch crude oil pipeline ruptured on December 4, <br /> 2003 at the subject site, releasing an estimated 750 barrels of crude oil to site soil (approximately <br /> 31,500 gallons). The pipeline carries crude oil from oil fields near Bakersfield to refineries in the <br /> Bay Area. The pipeline was reportedly ruptured during ripping of the soil for agricultural <br /> purposes. <br /> l Chevron subsequently conducted emergency response activities in an attempt to limit migration <br /> J of crude oil. Chevron reportedly created soil berms to restrict lateral migration of oil, recovered <br /> free oil with a vacuum truck and removed oil-impacted soil. Chevron estimated that <br /> approximately 400 barrels were recovered (16,800 gallons) and that approximately 350 barrels <br /> still remain in onsite soil at the site (14,700 gallons) at that time. Based upon aerial photos <br /> (provided by Chevron shortly after the release) of the spill area, it appears the largest amount of <br /> 1 oil settled to the east and northeast of the rupture following the crop lines and surface <br /> topography. <br /> jSan Joaquin County Environmental Health Division (SJC/EHD) requested a workplan for the <br /> ` purpose of assessing the limits of contaminated soils and groundwater quality beneath the site. <br /> That workplan (File no. 42428 / ST04P118) was written by Kleinfelder, dated March 22, 2004 <br /> and was submitted to SJC/EHD for review and comment. This workplan was subsequently <br /> approved by SJC/EHD. This document details Kleinfelder's findings from implementation of <br /> that workplan. <br /> On May 19 and 20, 2004, a pushprobe soil and groundwater assessment was conducted. A total <br /> 3 of twenty nine (29) push probes were advanced during the field activities. A total of twenty two <br /> `j 4-point composite soil samples, 26 discrete soil samples and four groundwater samples were <br /> submitted for chemical analyses for purgeable and extactable petroleum hydrocarbons and <br /> benzene, toluene, ethylbenzene, and xylenes (BTEX) compounds. Twenty five (25) shallow probes <br /> were advanced to total depths ranging from approximately 8 to 24 feet below ground surface <br /> (bgs). Four deeper groundwater pushprobes were advanced to total depths ranging from 44 to 58 <br /> l feet bgs. Groundwater was noted approximately 43 feet bgs in these four deeper borings. <br /> rJ <br /> A summary of Kleinfelder's findings are summarized as follows: <br /> J 1) Twelve discrete soil samples were collected and analyzed from perimeter pushprobe <br /> borings at depths ranging from 5 to 43 feet bgs. Based on this data, it is Kleinfelder's <br /> opinion that petroleum impacted soil has not migrated laterally a significant distance <br /> ` beyond the footprint area. Please note this finding does not include potential soil vapor <br /> - migration of volatile compounds, since soil vapor sampling was not conducted as part of <br /> this assessment. <br /> ` 2) A total of four grab groundwater samples were collected, one in the footprint area and <br /> three from perimeter locations. Relatively low concentrations of petroleum constituents <br /> 4-4843.T03IST04R1025 Pagel of 16 <br /> Copyright 2004 Kleinfelder,Inc. August 6,2004 <br />
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