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FORM +oa SUnhIUT IN DUPLICATE <br /> RTAT{OF uuFORM,, <br /> . n{FPRTM{MT OI MATY RAYnOOUMtp �'(/' <br /> DIVISION OF OIL AND GAS <br /> e '77- 2012- 7 History of Oil or Gas Well <br /> _ .i <br /> OPOLATol Great Basins Petroleum Co Fmrn Vernalis Gas Field <br /> Well No 9 T. 3S A,6E <br /> T.L.&W 026-9 M.D. n, g M. <br /> • See.- --_, , <br /> Dace August 12 1982 Signed_ ,/t9g/� <br /> 1801 Avenue of the Stars, Ste 1011 arles W. Hatten <br /> Los Angeles. fA 90067 _ (219) 879-0666 rdc President <br /> (A .I (Tale,Vaa N�) <br /> (t+edae SonaeT w Aaa•) <br /> It is n(the[raacse importance to be.a a complete pi 6ismn e( c t�e(l.Ur cbis (Orm w report a full edune of impernOe Operations tonesthe <br /> drilling and [vain[of [he rdl ee duriOs ._drilling, aleerin[ of eriv s, plu gins er th <br /> abandonment .i[h the dace che,erof. Be •use to md [aule sueb c®e <br /> laical psoduerioa dam tGT decades, amoOau of<emeat uud, top and bccmm of p1Yp, perforaeioa deeai4, sidecrackd iOnk. 1,Aian <br /> a[ [ems aboosinp d <br /> Dm <br /> 8-9-82 Moved in Jack Owens Rig 05, rigged up & filled hole with lease water. Hole taking <br /> fluid. Removed Xmas Tree, installed 6" Series 900 Dbl. Ram and Hydril BOPE. Unland <br /> tbg and remove tbg donut. Rig up &,circ out sand. Hole taking fluid. Circ. & <br /> clean up hole. Pulled out of hole. Rigged up Cogco Wireline Truck, ran in and set <br /> bridge plug at 3940' . Checked measurements with collar locator. OK. Pulled out & <br /> rigged down Cogco. Ran in hole with 2-3/8" 4. 70 J-55 tbg, hung tbg at 3798' KB, <br /> Removed BOPE and installed Xmas tree. Rig up and swab fluid to 3200' . Shut down at <br /> 3:00 AM. <br /> 8-10-82 Crew on location 6:45 AM. Cogco arrived 7:00 AM. RU Cogco, ran in and ran Nuclear <br /> Log from 3940-3794' . Tagged bridge plug at 3940' , checked collars at 3912, 3874' , & <br /> 3838' . Pulled out & laid down Nuclear Log and collar locator. RU steel carrier <br /> perforating gun 1-9/16" OD. Ran in & perfd 4' " csg from 3925-3918' with 4 holes/ft. <br /> All measurements checked OK. (First gun did not fire.) Used 3000 psi lubricates & <br /> grease gun. No immediate pressure response. Pulled out & laid down Cogco. Pressure <br /> commenced building up slowly. Released Jack Owens Rig 12:00 noon. At 3:00 PM csg <br /> pressure 1000 psi. Opened well & flowed water & gas for 1 hr. SI for night. <br /> 8-11-89 At 7:00 AM SITP 1460 psi, SICP 1500 psi. Turned well into production unit. Control <br /> regulator would not hold. Shut in well. Replaced regulator. 10:30 AM put well <br /> on production at 120 MCF rate. <br /> 8-12-82 At 9:30 AM: Flowing 156 MCF/D rate. FTP = 1275 psi, FCP = 1300 psi. <br /> 8-13-82 At 9:00 AM: Flowing 185 MCF/D rate. FTP = 1400 psi, FCP = 1410 psi. <br /> Vernalis Field went on PG&E. Deliverability test 9:00 AM 8/13/82. <br />