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4 <br /> HALLIBURTON SERVICES 5500 MIND AVlNUE,eUiTE 365 <br /> 13AKER9FIELD,CALIFOA141A 93309 <br /> (605)6:37.2971 <br /> June 19 , 1990 <br /> BKS-pU-168-90 <br /> Mr . Terry Kloth <br /> p$STEC Energy <br /> 34759 Lencioni Ave <br /> Bakersfield, Calif . 93308 <br /> RE: San Joaquin COGEN LTD <br /> Cogen N1 RD #1 <br /> pescaderoFieldnty, CA • <br /> San Joaquin <br /> Dear Terry : <br /> Halliburton Services is pleased to present the folelcian into wing dure <br /> the <br /> to acidize the referenced well to improve inj <br /> Lathrop Sands - <br /> Perfs : 8574-86 ; 8611-187 28-36; 8690-8729 ; <br /> 36-52 ; 68-94 ; 8916-40; 66-9018 ; <br /> 54-62 ; 70-9100 ; 9180-9227 ; 32-47 ; <br /> 60-983 9304-26 ; 43-51 ; 60-78 ; <br /> 9385-9413 ; 20-36 ; 44-58 ; 64-80 ;` <br /> 9485-9500 ; 20-48 ; 65-75 ft ( 503 ft net) <br /> BHST: 226` F <br /> ;a <br /> Casing: 7" , 26-29N <br /> Tubinq : 2-7/811 <br /> g C D D E'- <br /> 1 , HIH with coiled tubing to 9575 ft- <br /> 2 . Spot 1700 gallons 15% HCl-Fe Acid with 2% Clayfix. <br /> 3 , pull C-T to top of acid and displace the wellbore with 7% <br /> Clayfix • <br /> onnx with C-T and let acid soak 2-3 hours . <br />