Laserfiche WebLink
' Portions of the three samples were mixed with potable water from the site <br /> and it was demonstrated that a black colored residue formed and floated on <br /> ' free water from both the pure pozzolan and 50:50 cement/Pozmix® A. This <br /> demonstration is shown in photograph #13, Figure 4. <br /> ' The hot water, high-pressure cleaner on the BSK drill rig was used to clean <br /> Halliburton's pump truck (RCM®). The water sample collected from the <br /> pump truck was delivered by the BSK project manager to Chromalab, Inc., a <br /> State-certified laboratory, for TPH-Diesel analysis. The sample was released <br /> to Chromalab under a Chain-of-Custody Record. <br /> The SJPHS inspector called Halliburton's office in Woodland to inform them <br /> that under a 'RVotice to Abate" '(copy attached in Appendix A) to: 1) <br /> discontinue use of cement/Pozmix® A and 2) not grout additional wells unless <br /> the grout mix changed to cement plus three to five percent bentonite. Also, <br /> the inspector left a message at the BSK Pleasanton office for the project <br /> manager. At approximately 16:30, the BSK project manager called the SJPHS <br /> inspector and BSK was informed of the 'Notice to Abate" and that mixing of <br /> the grout was not to start until SJPHS approved the water supply. The <br /> inspector indicated he would be on site at 8:00 on June 3 to approve the <br /> mixing water supply. <br /> 3.3 June 3 Activities - The Halliburton twin-bin grout mix truck was on site prior <br /> to 08:00 with a 96 percent portland cement and four percent bentonite mix. <br /> Just prior to 08:00, the SJPHS inspector approved use of the water on the <br /> RCM® trailer. A BSK representative collected a water sample from the <br /> bottom discharge in a one liter amber colored glass jar. The jar was labeled <br /> Sample #2 Pump Water and placed in an ice chest with ice. <br /> ' The equipment was set up over MW-4 and the drill stem and bit assembly <br /> were positioned at 55 feet below the top of the well casing (see photograph <br /> 1 #14, Figure 4). Cement grout was pumped to fill the casing and then the drill <br /> stem was pulled so the jet bit was at 43 feet. The PVC well screen was <br /> perforated at this interval with grout overflow being directed to a containment <br /> pool (see photograph #15, Figure 4). Density measurements were taken in <br /> the field of both the grout mix before perforation and return flow grout using <br /> a Mud Scale (see photograph #16, Figure 4). In addition, two-inch by four- <br /> inch grout cylinders were cast in plastic molds of both original grout mix and <br /> overflow grout. The remainder of the perforations were completed as <br /> proposed in the Work Plan. The final perforation at three feet was completed <br /> ' at 10:17. The abandonment of MW-4 was completed under the observation <br /> of the SJPHS inspector. Two containment pools were used to store overflow <br /> grout. <br /> ' Prior to starting the abandonment operations for MW-6, Halliburton washed <br /> down the pumping equipment as a precaution so that operations would not <br /> ' have to be interrupted during completion of this well. Since the casing <br /> 7 <br /> &Associates <br />