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FORM 103 SUBMIT IN DUPLICATE $2803-70e a-vs 20M OO o.r <br /> RESOURCES AGENCY OF CALIFORNt <br /> DEPARTMENT OF CONSERVATION DIVISION OF OIL AND GAS <br /> DIVISION OF OIL AND GAS R E r r I `i c p <br /> History of Oil or Gas Well P P P 1 n W4 <br /> WOODLAIvO, CALIFORNIA <br /> UN1Ll1l- rG ���tl--��---'�.'-�.G�--------------• <br /> Well No.---Y_94lada__Inl----------------------- --., Sec.---29--------- T-2.5 11.7a------------ - ---------B,_D*B. & f. <br /> Date._SQyt_=b_Qr---4----------------- 19-14- Signed-------------------------- <br /> Ronald D. Leineke <br /> -X824--------------Title-----1? '-sillint------------------------------------------- <br /> (Address) (Telephone Number) (President,Secretary or Agent) <br /> History must be complete in all detail. Use this form to report all operations during drilling and testing of the well or during redrilling <br /> or altering the casing,plugging,or abandonment with the dates thereof. Include such items as hole size,formation test details,amounts <br /> of cement used, top and bottom of plugs,perforation details,sidetracked junk, bailing tests and initial production data. <br /> Date <br /> 1974 <br /> 8-23 hove in and rig up Hunnicutt & Camp Rig #5. Toolpusher John Smith. <br /> 8-24 Spudded 12k" hole at 1:OOAP4 and drilled to 668' , KB measurements, by 6:00xm. <br /> Ran 23 joints (669.991 ) of new 8 5/8" Kaiser 241b casing w/hol;CO cement <br /> guide shoe ( 1,001 ) and float insert with fill-up attachment placed in top <br /> of shoe joint at 638' , cemented with 240 sacks of Class"G" w/4o gel and <br /> 2;6 calcium chloride followed by 150 sacks of Class "G" W/2,*/ Calcium chloride. <br /> Zion 20 cubic feet of water ahead of cement and displaced with 228 cubic feet <br /> of water. Dumped top vrip er plug with 1100psi released pressure and no bleed <br /> back, Used Halliburton ':geld-A on guide shoe and first collar and one <br /> centralizer latched over the first collar. Surface casing set at 6681isl3. <br /> Good returns to surface on cement job. Installed casing head and tested <br /> welds w/3000psi for 30 min. , installed B.O.P.E. and tested blind rams <br /> w/1500psi, picked up 680" drill assembly and ran down to top of cement at <br /> 629' , tested pipe rams w/1500psi, tested Hydril and Kelly stop w/t000psi. <br /> 8-25 Ltarted drilling out with %II bit at 1:306MM. 8:OOAM dgilling at 16681, <br /> ;�iud wt. 720 vis. 41, W.L. 11.5, surveys 1 15'3668', 1 ;@16981 , 1°32896' . <br /> 8-26 8:00AM drilling 6�" hole at 38971, Mud wt. 73, Vise 439 W.L. 8.5 <br /> Survey 0 15134245' <br /> 8-27 8:OOAM Tipping for new 6;" bit at 475918 -cud wt. 73, Vise 39, 11J.L. 5,29 <br /> Survey 1 24759' <br /> 8-26 8:OOAM d5lling 6y" hole at 54711 , Mud wt, 74-J, Vis. 39, �:.L. 4.6 <br /> surveys 2C63041 , 1°C:5619' <br /> 8-29 8:00AM TE* ping for new 680" bit at 60581, laud wt. 75, Vis. 44, �t.L. 5.0 <br /> survey 3 30'Q6058' <br /> 8-30 -Drilled %II hole to T,D. 6380' by 2:JOAM. Ran Welex Induction-Electric Log. <br /> Total depth driller 6380' logger 63861. Plugged and Abandoned well as follows <br /> Plug#l: -1411 drill pipe hung at 718'H0'k:C0 equalized 95 sacks Class'IG" cement <br /> with 3% calcium chloride CIP Q, 3:30PIM, 7:OOPM located top of plug 9 460' <br /> Witnessed and approved by DOG. <br /> Plug; 25' surface plug vrith 10 sacks, <br /> Cut off 8 5/8" surface casing 5' below ground. Rig released at 12:OOPM <br />