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Soil Excavation and Second Quarter Post-Treatment Monitoring and Sampling Report 3 <br /> 46 The Southland Corporation,Store#20344,455 Grant i�ne Road,Tracy,CA ._ _June 9,1998 <br /> 13 Permitting/Srte-Specrfic Health And Safety Plan <br /> Fluor Daniel GTI conducted a technical review of all relevant information provided before proceeding with <br /> site assessment work Permits for the destruction three groundwater monitoring wells(MW-8,MW-9,MW- <br /> 10) and one groundwater extraction well (GWE-3)and installation of the one groundwater monitoring well <br /> (MW-16)were obtained from the SJCPHS (Appendix A) Following a complete review of site conditions, <br /> Fluor Daniel GTI revised the existing site-specific Heafth and Safety Plan to include any new safety <br /> concerns as required by the Occupational Safety and Health Administration (OSHA) Standard"Hazardous <br /> Waste Operations and Emergency Response"guidelines(29 CFR 1910 120) The document was <br /> reviewed and signed by all Fluor Daniel GTI personnel and subcontractors prior to commencement of work <br /> at the site <br /> i <br /> 2 0 WELL DESTRUCTION <br /> On April 27, 1998, Fluor Daniel GTI personnel supervised the destruction of three groundwater monitoring <br /> wells(MW-8,MW-9, MW-10)and one groundwater extraction well (GWE-3) The wells were destroyed to <br /> allow for the proposed soil excavation Prior to well destruction, each well was gauged for total depth and <br /> cleared of any obstructions Field notes are included as Appendix B <br /> . The four wells were destroyed by pressure grouting The well casings were grouted with Portland cement <br /> using a 1-inch diameter tremie pipe Fallowing placement of the grout inside the well casing, approximately <br /> 30 psi of air pressure was applied to the top of each casing using and air compressor <br /> During the excavation,the approximately top 9 feet(total depth of excavation) of each well casing along <br /> with the well traffic box and/or vault and associated concrete were removed with a backhoe bucket <br /> In addition, all horizontal piping extending from the monitoring wells and groundwater extraction wells to the <br /> former treatment system compound were grouted with Portland cement All piping within the area of the <br /> excavation was removed All well vaults,with the exception of GWE-2, were removed with a backhoe <br /> bucket The four-inch diameter effluent discharge line extending from the treatment system compound to <br /> the storm drain was capped at the eastern edge of the excavation near the concrete walkway in front of the <br /> store building <br /> 3 0 SOIL EXCAVATION <br /> On April 28, 29, and 30, 1998,Fluor Daniel GTI personnel supervised the excavation of hydrocarbon- <br /> containing sod northeast of the former UST pit and beneath the former fuel dispenser island to a depth of 8 <br /> to 9 fest BGS (Figure 2) A total of approximately 270 cubic yards or 345 tons of sod was excavated from <br /> the two excavations Soil was loaded directly onto trucks and transported to TPS Technologies in <br /> • Richmond, CA for proper treatment and disposal Soil transportation manifests are included in Appendix C <br /> FLUOR DANIEL GTI <br /> 2o3o"r.rpt 1�5_ <br />