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ARCO Meeting Minute <br /> August 8, 1994 <br /> a <br /> Page 4 <br /> ARCO 2076, Lodi (Mary Meays) <br /> Mary said that she had received the first quarter status'report and brought to our attention that <br /> total xylenes was detected in MW-3 during the fourth quarter of 1993. EMCON stated that the <br /> reported concentration was 0.7 ppb which is below MCLS and contamination could have easily <br /> occurred in the laboratory (dirty glassware,cross contamination, etc.). In addition,this was the <br /> only sampling event in over a year which resulted in the detection of hydrocarbons in <br /> groundwater. Laboratory results on groundwater samples collected during the first and second <br /> quarter of 1994 confirm that hydrocarbons are not present in the groundwater. <br /> Mary asked when ARCO would be scheduling remediation of the impacted soil. ARCO stated <br /> that a select number of abatement units have been allocated for San Joaquin County, and that <br /> ARCO intends to focus remediation efforts on those sites which have the highest amount of <br /> contamination or pose the greatest risk to groundwater,and therefore anticipate remediation of <br /> the site to begin after six months. ARCO explained to Mary that this schedule was dependent on <br /> the availability and performance of remediation systems operating in the county. <br /> ARCO 548,Stockton, (Mary Meays) <br /> Mary said that she had received the quarterly status report/PAR and that the PAR was deficient <br /> in areas outlined in her correspondence to ARCO and requested additional information (cross <br /> sections, remedial alternatives, VET results, etc.). EMCON submitted an addendum to the PAR <br /> at the meeting presenting this additional information. EMCON explained to Mary that based on <br /> conversations with her, an abbreviated PAR would be excepted since only a limited amount of <br /> data had been collected since submitting the Preliminary Investigation and Evaluation Report. <br /> Mary said that this was now not the case and complete PAR was required. EMCON told Mary <br /> that the addendum that was submitted that date should satisfy all PAR requirements. <br /> Mary said that based on the first quarter status report, it appears that dissolved hydrocarbon <br /> concentrations have increased and extend off-site. ARCO stated that the results of the first <br /> quarter sampling event may not accurately present the groundwater quality. ARCO explained to <br /> Mary that ARCO begin using a new groundwater sampling contractor the beginning of 1994 and <br /> data collected from some sites are likely inoorrect. EMCON informed Mary that the results of <br /> second quarter sampling event show that the concentrations are back to levels that are <br /> consistent with previous quarters and that hydrocarbons do not extend off-site. Mary said that <br /> she will review that data once she has received the report. <br /> Mary asked ARCO if the source has been eliminated and implied that there is an ongoing leak <br /> from the tanks. ARCO replied by saying that the tanks and lines have been tested and are within <br /> the allotted parameters. Mary questioned the general validity of tank testing stating that the tests <br /> are not accurate and is sure that leakage is occurring. Diane Hinson redirected the discussion <br /> stating that the dialogue was based on conjecture. <br /> Mary asked ARCO what type of remediation efforts were planned and when they would be <br /> implemented. EMCON stated that remediation by soil vapor extraction appears to be the most <br /> effective remedial alternative. Mary asked how groundwater was going to be remediated. <br /> EMCON said that the majority of dissolved hydrocarbons are located in the vicinity of the USTs <br /> and within the effective radius of influence of the vapor extraction system. ARCO said that <br /> remediation of groundwater was not going to be ignored and will monitor the effects the vapor <br /> extraction system has on the groundwater. Active groundwater remediation (pump and treat, air <br /> sparging, etc.) will not be implemented at this time but the need will be evaluated during <br /> operation of the vapor extraction system and be discussed in future quarterly status reports. <br />