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1+ I <br /> ERT 205513 QSR23 76 Facility 5886,Stockton,California January 30,2003 <br /> . • During second quarter 2000, ERI installed one UST cavity well in general accordance with the <br /> CAP(ERI, December 28, 1999)and Tosca initiated periodic purging of groundwater from the <br /> UST cavity well and from groundwater monitoring well MW3 Groundwater purging was <br /> temporarily discontinued during third quarter 2000 pending clarification from the County <br /> regarding water sampling and data collection requirements Purging was resumed during January <br /> 2001,and continued through January 2002, when it was terminated following installation and <br /> operation of the microsparge remediation system Approximately 285,000 gallons of groundwater <br /> were purged from the UST cavity well and well MW3 and transported to the Tosco refinery for <br /> recycling during interim groundwater remediation efforts <br /> • During June 2001,Tracer Research Corporation(TRC)performed an enhanced leak detection test <br /> on underground storage systems to evaluate the system integrity According to Tosco, the results <br /> of the enhanced detection test indicated that the underground storage systems are functioning <br /> within acceptable parameters <br /> • During third quarter 2001, ERI submitted a CAP, dated September 25,2001 The CAP included <br /> recommendations to install a microsparge system to remediate MTBE impacted groundwater <br /> beneath the site <br /> During first quarter 2002, the rmcrosparge remediation system was completed and ERI performed <br /> system startup and initiated monthly operation and maintenance(O&M) of the system <br /> Currently, there are ten on-site AS wells(ASI through AS5,AS7,AS8, and AS 10, and nested wells <br /> . AS6S/D and AS9S/D),three on-site, single-casing groundwater monitoring wells(MW 1 through MW3), <br /> four on-site, dual-casing groundwater monitoring wells(MW4S/D through MW7S/D), one on-site UST <br /> cavity well, and nine off-site groundwater monitoring wells(MW8S/I/D through MW10S/I/D)consisting <br /> of three wells at each nested well location as shown on Plate 2 and the On-Site Well Locations(Plate 3) <br /> Prior to fourth quarter 2002, data collected during quarterly groundwater monitoring and sampling events <br /> indicated dissolved hydrocarbons were effectively delineated both laterally and vertically in the vicinity of <br /> the site However, laboratory analysis of samples collected in November 2002 detected minor <br /> concentrations of MTBE ranging from 2 6 to 9 5 ppb (parts per billion) in groundwater from downgradient <br /> off-site wells MW8D and MW 101/1) In addition,dissolved hydrocarbons continue to be detected in <br /> groundwater samples collected from on-site wells and are concentrated in the vicinity and downgradient of <br /> the UST cavity <br /> FOURTH QUARTER 2002 ACTIVITIES <br /> Based upon previous work completed at the site, and in accordance with the correspondence and request <br /> from the County, the following tasks were performed during the fourth quarter 2002 <br /> • ERI performed monthly remediation system O&M and collected monthly groundwater samples <br /> from wells MW 1 through MW3 <br /> 3 <br />