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ARCHIVED REPORTS_XR0005148
EnvironmentalHealth
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2900 - Site Mitigation Program
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PR0535112
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ARCHIVED REPORTS_XR0005148
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Last modified
9/23/2020 11:58:57 PM
Creation date
3/17/2020 3:00:33 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0005148
RECORD_ID
PR0535112
PE
2957
FACILITY_ID
FA0020296
FACILITY_NAME
CHAPIN BROTHERS INC
STREET_NUMBER
1766
STREET_NAME
MONTE DIABLO
STREET_TYPE
AVE
City
STOCKTON
Zip
95203
APN
13505050
CURRENT_STATUS
01
SITE_LOCATION
1766 MONTE DIABLO AVE
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
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EHD - Public
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J e <br /> M <br /> i <br /> 1 <br /> 28 April 1998 n <br /> AGE-NC-95-0103 <br /> ' Page 8 of 9 ! <br /> 1 1 <br /> ' from well MW-4 east of'the former gasoline USTs location Hydrocarbons were also <br /> detected at lesser concentrations in wells MWA, MW-3 and MW-5 Detectable <br /> concentrations hydrocarbons were not present in the samples collected from the off-site wells, <br /> ' MW-2 and MW-6 and no hydrocarbons were detected in newly installed well MW-7, east <br /> of well MW-4 <br /> • A reduction of the dissolved-phase hydrocarbon plume concentrations in the central portion <br /> of the site has occurred since the initiation of the remediation system Additionally, a <br /> reduction of hydrocarbon concentrations has occurred at the location of well MW-5 A slight <br /> decrease of hydrocarbon concentrations has occurred in the down-gradient well MW-3 <br /> during the last quarter A portion of the observed drop of dissolved hi drocarbons may be due <br /> to ground water being approximately 5 feet above the screened intervals of MW-1 through <br /> MW-4 <br /> r ' <br /> • DIPE was detected in water samples collected from MW-3 and MW-5, with a maximum <br /> concentration of 85 ppb in MW-5 MTBE was detected in samples collected from MW-1 and <br /> MW-4, with a maximum concentration of 55 ppb in MW-4 TBA was not detected in any <br /> groundwater samples this quarter <br /> Dunn g operation of the SVE system during this quarter, an estimated 65 gallons of gasoline <br /> E were removed from the site Since initiation of the SVE system an estimated-total of 381 <br /> gallons of gasoline have been removed E <br /> • I <br /> The'SVE system has removed a major portion of the hydrocarbons from the�adose soil zone <br /> in the SVE system's area of influence Soil contamination probably remains in saturated soil r <br /> in the core portion of the dissolved hydrocarbon plume ; <br /> J• Benzene concentrations in the extracted soil vapor has been reduced to concentrations bel ow <br /> r the detection limits of the soil vapor analytical method 8020 <br /> ! 11 1 <br /> I� 5.0. ' RECOMMENDATIONS , <br /> ased upon data collected over the quarter at site, AGE recommends the following <br /> ,1 stallation of additional IAS point or wells to stimulate remediation of impacted ground ' <br /> ater in the area of well MW-4 and the southeastern quadrant of the remediation area A E <br /> work plan for the installation of the sparge,points and costs have been approved 4 <br /> I ! u , 1 <br /> • perate of the SVE system drawing,vapors from the central portion of the site, which has ! <br /> ' emonstrated hydrocarbon-impacted soil vapor. The SVE should be operated for an <br /> J <br /> Y I Advanced GCOEnvironmental,Inc <br /> !I I <br />
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