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Advanced BORING LOG <br /> GeoEnvironmental, Inc. <br /> 1 r, BOREHOLE NO.MW-2 <br /> �s 837 Shaw Road, Stockton, CA 95215 <br /> (209)467-1006 FAX: (209)467-1118 TOTAL DEPTH: $Q' <br /> Project: Former Blue Star Gasoline Drilling Co.: Cascade Drilling,Inc. <br /> Site Location: 4040 East Main Street Rig/Auger Type: CME-75HT <br /> Stockton, California Logged By: Jo'l Chapman <br /> Reviewed By: Calvin Lee <br /> Project No.: AGE-NC-01-0886 <br /> Date(s) Drilled: 02 and 03 May 2005 <br /> Notes: sz Water level during drilling Page 1 of 2 <br /> s Water level in completed well <br /> Depth Sample Blows PID Soil USCS Class and Well Well <br /> ID (per 6") (ppm) Symbol Soil Description Completion Description <br /> 0 <br /> Well cover Cristy box <br /> –5 MW2-5 15/16/21 NM ML:Dark brown,CLAYEY SILT;moist,low <br /> plasticity,very high consistency,moderate toughness, <br /> no hydrocarbon(HC)odor. <br /> –10 MW2-10 15/15/22 NM MI.:Dark brown,CLAYEY SILT;moist,low <br /> plasticity,very high consistency,moderate toughness, <br /> no HC odor. <br /> –15 MW2-15 14/17/19 NM ML:Dark brown,CLAYEY SILT;moist,low <br /> plasticity,very high consistency,moderate toughness, <br /> no HC odor. <br /> Neat cement from 0.5'to <br /> ML:Brown,SILT;moist,low plasticity,low 56'bsg <br /> –20 MW2-20 14/15/20 NM consistency,low toughness,no HC odor. <br /> –25— MW2-25 17/17/22 NM ML:Dark brown,CLAYEY SILT;low plasticity, <br /> high consistency,moderate toughness,some pea <br /> gravel,no IIC odor. <br /> 2"Diameter,Schedule <br /> 40 PVC with 0.020" <br /> slotted screen <br /> –30 MW2-30 13/17/19 NM ML:Brown,SILT;moist,low plasticity,high <br /> consistency,low toughness,some pea gravel,no HC <br /> odor. <br /> –35— MW2-35 17/18/20 NM ML Dark brown,CLAYEY SILT;moist,low <br /> plasticity,high consistency,moderate toughness,no <br /> HC odor. <br /> –40 MW2-40 18/19/21 NM ML:Dark brown,CLAYEY SILT;moist,low <br /> plasticity,high consistency,moderate toughness,no <br /> HC odor. <br />