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V <br /> � F <br /> • Thrifty Oil Co. Station #172 <br /> Page3 <br /> In addition, vapor samples were collected on February 11, 2003 from selected well heads The well <br /> head, influent, and effluent vapor samples were analyzed for TPH-g by EPA method 8015, and <br /> BTEX/MTBE by EPA method 8021B Copies of the influent, effluent, and wellhead vapor sample <br /> laboratory analytical results are presented in Appendix D The effluent air sample results are within <br /> the San Joaquin Valley Air Pollution Control District requirements <br /> A historical summary of hydrocarbons removed by vapor extraction is presented in Table 3, vapor <br /> sample analytical results for the individual wells sampling are presented in Table 5 The Field <br /> Status Reports are included in Appendix C <br /> Groundwater Treatment System <br /> The groundwater treatment system was started in conjunction with the vapor treatment system on <br /> April 26, 2001, and the flow meter started at zero Presently, the remediation system is connected <br /> to groundwater wells MW-10 and MW-11 Two down-well pneumatic pumps (one in each well) <br /> draw water into a 150-gallon polyvinyl tank, which then transfers the water through two (2) one <br /> thousand-pound canisters with activated carbon <br /> . During this reporting period, the groundwater extraction system was down for repairs The operation <br /> of the groundwater system was resumed on April 9, 2003 after installation of a continuous LEL <br /> monitoring device that is interlocked with the control circuit of the groundwater pumping system, <br /> meeting the City of Stockton, Department of Municipal Utilities (CSDMU) new permit <br /> requirements As of June 27, 2002, a total of 93,114 gallons had been treated and discharged <br /> Historical groundwater system operations are reported in Table 4 <br /> Summary and Recommendations <br /> The soil vapor and groundwater extraction systems were started on April 26, 2001 A total of 64,292 <br /> pounds of hydrocarbons have been destroyed by the vapor extraction system, and 93,114 gallons of <br /> groundwater have been treated by the groundwater system The groundwater extraction system was <br /> non-operational throughout the quarter,because of system maintenance and new permit requirements <br /> from the CSDMU <br /> Thnfty believes that the contamination found in well MW-6 is either from cross-contamination <br /> during gauging and sampling or from an independent off-site source Thrifty will take extra <br /> precautions to avoid any possible cross-contamination during the next sampling event If the <br /> contamination is still found within the well during the next sampling event, it 1s a reasonable <br /> possibility that it is from another off-site source, because Thnfty has a non-detect well (MW-3) <br /> • between the on-site and off-site contamination <br />