TABLE 3
<br /> . Vapor Extraction Operating Data
<br /> Thrifty Oil Station # 472, Stockton, CA
<br /> 021, 4„ !0=MmaV v
<br /> uOcri s, [ ?fl ��
<br /> b ritit
<br /> �F �
<br /> W4118/02 7,802 165 202 F
<br /> 2 5 (ND) 11 05 142 0 29,366
<br /> 4125102 7 969 i67 202 11 05 14 29,367 System shut down(technician on vacation)
<br /> 519102 7,969 0 - 1105 00 29,367 Restarted
<br /> 5123102 8,014 45 211 11 05 04 29,368 Knockout switch shut down VES restarted
<br /> 5130/02 8 182 168 212 (ND) 25 (ND) 11 05 is 29 369
<br /> 6!6102 8,348 168 213 1105 15 29,370
<br /> 6!93102 8 517 169 236 11 05 16 29 372
<br /> 6/20102 8 683 166 216 1,120 4,960 3487 29,721
<br /> 6127102 8,854 171 213 4,960 6804 30 401
<br /> 713102 8,996 142 212 4,960 5598 30,961
<br /> 7110102 9 166 170 213 4 960 6701 31 631
<br /> 7118102 9,350 184 203 1,060 4,670 6892 32 320
<br /> 7125102 9,523 173 213 4,670 628 5 32,949
<br /> 811102 9 687 164 203 4,670 5958 33,545
<br /> 818102 9,847 160 203 4,670 5673 34,112
<br /> 8113102 9,963 116 203 4,670 411 3 34,523 System shut down for Q
<br /> 8114102 9,963 0 - 4 670 00 34 523 Restarted
<br /> 8115!02 9,976 13 201 712 2,910 370 34,560
<br /> 8122102 9 978 2 210 2 910 45 34 565 Found system off power failure restarted
<br /> 8!29102 10 147 169 203 2,910 3798 34 945
<br /> 915102 10,311 164 204 2,910 3632 35,308
<br /> 9112102 10 485 174 201 483 2 130 3321 35 640
<br /> 9119102 10,642 157 201 2,130 2514 35,891
<br /> 9/2fil02 10,811 169 201 2,130 2706 36 162
<br /> NOTE Inlet concentration Is obtained from laboratory analytical result for Total Petroleum Hydrocarbons(TPH)
<br /> and assumed the same until the subsequent sampling
<br /> 014tab3 Page 2 of 2 10/2/02
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