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ARCHIVED REPORTS_XR0006090
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ARCHIVED REPORTS_XR0006090
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Last modified
9/29/2020 10:11:17 PM
Creation date
4/17/2020 2:28:02 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0006090
RECORD_ID
PR0545603
PE
3528
FACILITY_ID
FA0006095
FACILITY_NAME
PETERSON MFG
STREET_NUMBER
2403
STREET_NAME
NAVY
STREET_TYPE
DR
City
STOCKTON
Zip
95206
CURRENT_STATUS
02
SITE_LOCATION
2403 NAVY DR
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
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SJGOV\sballwahn
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EHD - Public
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Ckv a <br /> A S S O C I A T E S I N C <br /> In July 1994, a RESNA field geologist observed the drilling of four additional groundwater <br /> monitoring wells (MW4, MW5, MW6, and MW7) at the site to further characterize subsurface <br /> conditions Groundwater samples collected from these additional wells contained no detectable <br /> petroleum hydrocarbons A detailed discussion of the Phase II Subsurface Investigation can be <br /> found in RESNA's "Summary Report, July 1994 Investigation,"dated August 26, 1994 <br /> In PHS/EHD correspondence dated March 1995, regulatory approval was given to sample wells <br /> MW3 and MW5 and wells MW4, MW6 and MW7 on an alternating semi-annual basis MW1 <br /> and MW2 were to be sampled every quarter, conditions permitting <br /> To further evaluate the extent of residual soil contamination in the vicinity of the former <br /> underground fuel storage tank (UST), Smith Technology supervised the advancement of four soil <br /> borings (SB-1, SB-2, SB-3, and SB-4) on February 29, 1996 to depths of approximately 16 to 26 <br /> feet bgs Total petroleum hydrocarbons as gasoline (TPHg), benzene, toluene, ethylbenzene, and <br /> xylenes (BTEX) were detected above method detection limits at low to moderate concentrations <br /> in samples collected at depths between 10 and 15 feet bgs in bonngs SB-1, SB-2, and SB-3 A <br /> detailed discussion of this subsurface investigation can be found in Smith Technology's <br /> "Subsurface Investigation Report, " dated April 30, 1996 <br /> . GROUNDWATER MONITORING AND SAMPLING <br /> ATC personnel performed groundwater monitoring and sampling on September 27, 1999 Field <br /> work consisted of measuring the depth-to-water in wells MW1 through MW7, using an <br /> electronic water/product interface probe to determine if free product was present, purging and <br /> sampling wells MW1 through MW7, and servicing the passive skimmer placed in well MW2 <br /> Static groundwater elevations were measured in each monitoring well on September 27, 1999 <br /> Groundwater was measured at an average of approximately 12 71 feet bgs, a decrease of 0 27 <br /> feet since last monitored in June 1999 A groundwater gradient map was created with the <br /> September 27, 1999 data using a computer kriging program The gradient map, presented as <br /> Figure 2, depicts a southwesterly groundwater gradient averaging 0 0006 ft/ft or approximately <br /> 16 feet/mile Groundwater monitoring data are summarized in Table 1 <br /> On September 27, 1999 groundwater samples were collected by ATC from monitoring wells <br /> MW1 though MW7 Groundwater samples were collected from the monitoring wells after <br /> stabilization of pH, electrical conductivity (EC), and temperature All wells monitored were <br /> purged and sampled according to our Quality Assurance/Quality Control Plan on file with the <br /> PHS/EHD A minimum of five casing volumes of water were removed from each sampled well <br /> A dedicated disposable bailer was used to collect each water sample Purge water was <br /> discharged to the sanitary sewer under permit Field parameters and purged volumes are shown <br /> • on well purge logs included in Attachment I <br /> 625811QUARTLWQR-1999 DOC 2 <br />
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