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ARCHIVED REPORTS_XR0008146
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3500 - Local Oversight Program
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ARCHIVED REPORTS_XR0008146
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Last modified
5/5/2020 3:22:34 PM
Creation date
5/5/2020 2:35:19 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0008146
RECORD_ID
PR0545641
PE
3528
FACILITY_ID
FA0002480
FACILITY_NAME
SHOP N GO 3
STREET_NUMBER
4511
STREET_NAME
PACIFIC
STREET_TYPE
AVE
City
STOCKTON
Zip
95207
APN
11023011
CURRENT_STATUS
02
SITE_LOCATION
4511 PACIFIC AVE
P_LOCATION
01
P_DISTRICT
002
QC Status
Approved
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EHD - Public
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' 06 August 2004 <br /> AGE-NC Project No 95-0128 <br />' Page 5 of 11 <br />' 2 3 3 Well Completions <br /> Pilot boring EW2 was completed using 6-Inch diameter PVC casing,with 0 03-inch slotted screen <br />' Installed from 35 to 55 feet bsg,VW2 through VW4 were completed as vapor extraction wells using <br /> 2-inch diameter PVC casing, with 0 02-Inch slotted screen Installed from 20 to 35 feet bsg, then a <br /> filter pack(No 3 Lonestar sand)was Installed from total depth to 2-feet above the slotted screen,and <br />' a nominal 2-foot bentonite chip plug was then Installed above the filter pack and hydrated The wells <br /> were then grouted to near the surface with portland cement,and water-tight,traffic-rated well boxes <br /> were Installed over the wells As-built well diagrams are depicted on the boring logs in Appendix C <br /> 1 <br /> 2 3 4 Laboratory Analysis of Soil Samples <br />' Selected soil samples were analyzed for <br /> • TPH-g and TPH-d in accordance with EPA Method 8015 Modified, and <br /> • BTEX and MTBE In accordance with EPA Method 8021 <br /> 1• <br /> 1 2 3 5 Extraction Well Development <br /> On 29 March 2004, ground water extraction well EW-2 was developed utilizing a Waterra Inertia <br /> 1 pump with a hose bailer Ground water was purged from the extraction well until ground water was <br /> visually sediment free, approximately 100 gallons of water were removed from the well Purged <br /> water was discharged into the active groundwater treatment system for treatment and disposal Field <br /> 1 sheets and data are Included in Appendix B <br /> 1 2 3 6 Well Elevation Head Survey <br /> On 30 March 2004,a California state-licensed surveying engineer from Baumbach and Piazza(BP) <br /> surveyed the elevation of monitoring wells MW-17, MW-18 and EW-2, the elevation at the top of <br /> the well casing was surveyed to the nearest 0 01-foot relative to Stockton benchmark #15, at an <br /> elevation of 10 98 feet above mean sea level (MSL) The results of the monitoring well survey are <br />' contained in Table 2 The surveying report by BP Is presented In Appendix D <br /> IAdvanced GeoEnvironmental Inc <br />
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