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ARCHIVED REPORTS_XR0009567
EnvironmentalHealth
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3500 - Local Oversight Program
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PR0545644
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ARCHIVED REPORTS_XR0009567
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Last modified
5/6/2020 10:14:54 AM
Creation date
5/6/2020 9:56:56 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0009567
RECORD_ID
PR0545644
PE
3528
FACILITY_ID
FA0003814
FACILITY_NAME
TOSCO CORPORATION #30878*
STREET_NUMBER
7303
STREET_NAME
PACIFIC
STREET_TYPE
AVE
City
STOCKTON
Zip
95207
APN
07736021
CURRENT_STATUS
02
SITE_LOCATION
7303 PACIFIC AVE
P_LOCATION
01
P_DISTRICT
002
QC Status
Approved
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EHD - Public
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. KEI-P89-1104 .QR2 <br /> August 7 , 1991 <br /> Page 5 <br /> static water level measured at 55 feet. The length of the existing <br /> casing could not be determined with the equipment on-site. <br /> Approximately 135 gallons of water were bailed from the water well <br /> using a clean stainless steel bailer. A water sample was obtained <br /> for analyses, and it was noted that the water sample contained <br /> sediment and what appeared to be iron flakes. The water sample was <br /> analyzed at Sequoia Analytical Laboratory in Redwood City, Califor- <br /> nia, on April 24 , 1990 for TPH as gasoline and BTX&E. The <br /> analytical results indicated non-detectable levels of TPH as <br /> gasoline and BTX&E, except for 0. 79 ppb of toluene. Mr. Harlin <br /> Knoll of the SJCPHS was informed of the results on May 10, 1990, <br /> and indicated that the ground water should be treated as contami- <br /> nated because of the detected toluene. <br /> West Hazmat only had 100 feet of the 12-inch O. D. augers available <br /> on-site on April 23 , 1990 , and therefore the well (135 feet deep) <br /> could not be fully drilled out and the casing removed from the <br /> ground. A phone call was placed from the field to Mrs. Diane <br /> Henson of the SJCPHS to determine if the work plan could be <br /> modified to allow the six-inch diameter well casing to remain in <br /> the ground and grout placed only on the inside of the casing for <br /> the full depth of the well . This modification to our work pian was <br /> verbally approved by Mrs. Henson. <br /> However, further evaluation of the surface area adjacent to the <br /> six-inch diameter well casing identified a second casing, approxi- <br /> mately 10 inches in diameter, around the six-inch diameter casing. <br /> The depth of the second casing could not be determined, and it was <br /> unclear if the annulus between the six and ten-inch diameter <br /> casings was backfilled or open. A second phone call was placed to <br /> Diane Henson on April 23 , 1990, and it was determined that only <br /> grouting of the inside of the six-inch casing would not necessarily <br /> provide an adequate seal to protect the ground water. Therefore, <br /> KEI was instructed not to destroy the water well at this time. <br /> The water well was provided with a temporary surface seal on April <br /> 23 , 1990, prior to leaving the site, by driving in a circular wood <br /> plug, pouring one sack of bentonite powder gel over the wood plug <br /> and vicinity, and placing cement over the bentonite gel. <br /> KEI contacted Purviance Drillers, Inc. of Linden, California, for <br /> a proposal to properly abandon the dual cased water well. It was <br /> initially proposed to Det out any materials within the annulus <br /> spacing between the two well casings, split the six-inch diameter <br /> casing with a dawn-the-hole perforator tool, and to place Baroid <br /> Aquagrout Benseal within the annulus and within the six-inch <br /> diameter casing for the full depth of the well, using a tremie <br /> tube. In addition, it was subsequently proposed to conduct a down- <br />
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