My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
ARCHIVED REPORTS_XR0007645
EnvironmentalHealth
>
EHD Program Facility Records by Street Name
>
T
>
TRACY
>
3725
>
2900 - Site Mitigation Program
>
PR0528359
>
ARCHIVED REPORTS_XR0007645
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
5/8/2020 3:46:24 PM
Creation date
5/8/2020 3:18:23 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0007645
RECORD_ID
PR0528359
PE
2950
FACILITY_ID
FA0019146
FACILITY_NAME
SHELL OIL PRODUCTS US
STREET_NUMBER
3725
Direction
N
STREET_NAME
TRACY
STREET_TYPE
BLVD
City
TRACY
Zip
95304
APN
21217030
CURRENT_STATUS
02
SITE_LOCATION
3725 N TRACY BLVD
P_LOCATION
03
P_DISTRICT
005
QC Status
Approved
Scanner
LSauers
Tags
EHD - Public
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
102
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
CAMBRIA SEP 032002 <br /> ENENT HEALTH <br /> pERMIMSERVICES <br /> August 30, 2002 <br /> Mr Harlin Knoll <br /> San Joaquin County Environmental Health Department <br /> Environmental Health Division <br /> 304 East Weber Avenue, Third Floor <br /> Stockton, California 95202 <br /> Re Groundwater Monitoring Report— Second Quarter 2002 <br /> Shell-branded Service Station <br /> 3725 Tracy Boulevard <br /> Tracy, California <br /> SAP Code 136186 <br /> Incident No 98996222 <br /> Dear Mr Knoll <br /> Cambria Environmental Technology, Inc (Cambria) prepared this report on behalf of Equilon <br /> Enterprises LLC dba Shell Oil Products US (Shell) in accordance with quarterly reporting <br /> requirements of 23 CCR 2652d <br /> SECOND QUARTER 2002 ACTIVITIES <br /> Groundwater Monitoring. Blaine Tech Services, Inc (Blaine) of San Jose, California gauged <br /> and sampled all site wells and prepared a summary table of field gauging data and laboratory <br /> analytical results These activities were coordinated with the Chevron service station located at <br /> 3775 Tracy Boulevard Cambria prepared a site vicinity/well survey map (Figure 1), and a <br /> groundwater contour/chemical concentration map (Figure 2) Cambria also prepared a graph <br /> (Figure 3) which is a plot of MTBE concentration in monitoring well MW-1A versus time <br /> Cumulative mass removed is also shown on the graph Blaine's report, which includes the <br /> laboratory report, is included as Appendix A Available well gauging data for the Chevron <br /> station is included in Appendix B <br /> Groundwater Remediation Monthly groundwater extraction (GWE) using a vacuum truck <br /> Oakland [A began February 7, 2000 During May 2001 the frequency of GWE was increased to twice a <br /> San Ramon CA month Between April 3, 2002 and June 24, 2002, a total of 18,111 gallons of groundwater was <br /> Sonoma CA removed from well MW-1A A summary of the volume of groundwater extracted at the site and <br /> Cambria an estimate of the amount of total purgeable hydrocarbons as gasoline (TPHg), benzene, and <br /> Environmental methyl tertiary butyl ether (MTBE)removed is presented in Table 1 <br /> Technology, Inc <br />_18erkins Street <br /> PO Box 259 <br /> Sonoma CA 95476 <br /> Tel(707)935-4850 <br /> Fax(707)935-6649 <br />
The URL can be used to link to this page
Your browser does not support the video tag.