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ARCHIVED REPORTS_XR0007645
EnvironmentalHealth
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2900 - Site Mitigation Program
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PR0528359
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ARCHIVED REPORTS_XR0007645
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Entry Properties
Last modified
5/8/2020 3:46:24 PM
Creation date
5/8/2020 3:18:23 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0007645
RECORD_ID
PR0528359
PE
2950
FACILITY_ID
FA0019146
FACILITY_NAME
SHELL OIL PRODUCTS US
STREET_NUMBER
3725
Direction
N
STREET_NAME
TRACY
STREET_TYPE
BLVD
City
TRACY
Zip
95304
APN
21217030
CURRENT_STATUS
02
SITE_LOCATION
3725 N TRACY BLVD
P_LOCATION
03
P_DISTRICT
005
QC Status
Approved
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LSauers
Tags
EHD - Public
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Rugtt12 02 a8: 04a p. 2 <br /> �f1 Irk <br /> Water Well Technology, Inc. <br /> License No C57 Tal M <br /> P O Box 519 Fair Oaks,Ca 95628 <br /> 6 (800)961-WELL (916)961 9355 Fax (916) 961-1773 <br /> August 7, 2002 VISUALWELL LOG <br /> Cambria Environmental <br /> Well Shell 3725 Tracy Boulevard <br /> o Casino s a0 6 in <br /> 7' Static W2te, _eval;clear) <br /> .i -Pavyincrustatio, REASON FOR VIDEO <br /> 20 <br /> jr Check condition for abandonment <br /> 'Y ]etenoration and holes <br /> AREA VIEWED <br /> c Ground to 115 ft <br /> 40 EVALUATION FROM SURVEY <br /> ;4 Casing Poor condition /thin and deteriorated /heavy incrustation <br /> Y Perforations Vertical slots/ few visible due to encrustation <br /> ,X Total depth 115 ft <br /> 60 X <br /> AREAS OF CONCERN <br /> X 1)Old cable tool well, likely does not have a proper surface seal <br /> -;- 2) Plugged perforation <br /> 8° 3)Deterioration due to age of casing <br /> NOTES & SUGGESTIONS <br /> Due to condition of casing it would be better to blast perforate with <br /> sealing ma eriaf in the well rather then mechanical perforate and have <br /> too caving or stuck tools <br /> t, 107 io 115 181 Perforations <br /> 115 Bclon <br /> 120 Dnlieo deolh unamctivn <br /> SURVEY BY Renee <br /> EVALUATION BY Robert J Guardino <br /> It you have any questions regarding this report <br /> please call 91 6 961 9355 <br /> The accuracy of this report is oased on the video survey and information given to WWTI The comments and <br /> recommendations are the opoions of WWTI based on this information Other information not known to WWrl <br /> may change the opinions expressed in this report <br />
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