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CLEANUP AND ABATEMENT ORIIER NO. 5-01-703 • <br /> CITY OF RIVERBANK WASTEWATER TREATMENT PLANT - <br /> STANISLAUS COUNTY <br /> the facility. Staff has detennined that the proposed discharge modification would violate the <br /> RBAAP Record of Decision and pose a threat to groundwater quality at the facility. RBAAP has <br /> been notified of this determination. <br /> 7. Influent flow to the facility is typically highest in the summer due to the cannery discharge. Order <br /> No. 94-100 prescribes an average daily dry weather flow of 7.9 mgd. In 1999, the peak daily flow <br /> was 5.9 mgd and the average daily flow was 2.1 mgd. In 2000, the peak daily flow was 5.7 mgd <br /> and the average daily flow was 2.3 mgd. <br /> 8. In 1996, the Discharger applied for a State Revolving Fund loan to finance facility improvements. <br /> The purpose of the project is to prevent odor problems during the tomato processing season, <br /> provide a separate treatment cell for winter flows to allow emptying and cleaning of the Summer <br /> Aeration Cell, and prevent overflows at the headworks. The project as approved includes <br /> replacing the plant's motor control center, which was inadequate to provide reliable power for the <br /> aerators. Several aging aerators were to be replaced, and additional aerators were to be added to <br /> restore treatment capacity to the Winter Aeration Pond. The project also included reconstruction <br /> of the plant headworks to eliminate the hydraulic bottleneck caused by the current solids screening <br /> system. The State Water Resources Control Board approved the Discharger's Facilities Plan on <br /> 29 March 2000. <br /> 9. As a separate project with funding provided by the City of Riverbank, the Discharger undertook a <br /> stone water segregation project to provide separate storm drains for the older part of the City, <br /> which is currently served by a combined sewer. During heavy precipitation events, the combined <br /> sewer discharges hydraulic loads that can overwhelm the headworks. The purpose of the project is <br /> to reduce winter flows and potential headworks overflows during high-precipitation events. <br /> 10. On 10 September 1999, staff received the Discharger's verbal report of a spill of untreated waste <br /> from the plant headworks that occurred on 6 September 1999. The spill was caused by ari <br /> electrical overload that stopped the screening mechanism within the headworks. Approximately <br /> 10,000 gallons of raw sewage (primarily tomato processing waste)was discharged to a contained <br /> land area below the headworks. The discharger cleaned out and disinfected the spill area as soon <br /> as practical after power was restored to the headworks. The Discharger also installed an auto <br /> dialer alarm system to inform the treatment plant operator of headworks power failure. A Notice <br /> of Violation (NOV) was issued for the spill on 15 November 1999. <br /> 11. On 25 January 2000, the Discharger reported that the headworks overflowed during a high- <br /> precipitation event due to sewer flows in excess of the headworks hydraulic capacity. <br /> Approximately 40,000 gallons of raw sewage diluted with storm water runoff was discharged to <br /> the contained land area below the headworks. Once equipment access was possible, the <br /> Discharger pumped the effluent back to the headworks and disinfected the spill area. Staff <br /> understands that most of the waste percolated into the ground. <br /> 12. An NOV was issued for this violation on 4 February 2000. The NOV required that the Discharger <br /> submit a report that specified the timeline for completion of the storm drain segregation project. <br /> The Discharger stated that the electrical improvements and some of the replacement aerators <br /> would be completed by August 2000, and that the storm drain segregation project would probably <br /> be completed in 2000. <br />