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1260 Graphics Drive <br /> CV <br /> Modesto California <br /> 95351 <br /> F _ 209 579 2221 <br /> Fax 209 579 2225 <br /> A 8 S O C I A T E S I N C r, 0 <br /> September 9, 1998 <br /> 62605 <br /> Mr Ron Rowe <br /> San Joaquin County Public Health Services <br /> Environmental Health Division <br /> 304 E Weber Street, Third Floor <br /> Stockton, California 95202 <br /> Subject Monitoring Report Third Quarter 1998, Former Thiemann's Service Station, 106 <br /> West Second Street, Ripon, California <br /> Dear Mr Rowe <br /> This report presents the results of quarterly groundwater monitoring and sampling performed in <br /> July 1998 by ATC Associates Inc at Former Thiemann's Service Station The site is located at <br /> 106 West Second Street in Ripon, California (Figure 1) Sampling was performed to monitor the <br /> distribution of petroleum hydrocarbons in groundwater at the site Monitoring was performed to <br /> determine the groundwater flow direction and the hydraulic gradient in the uppermost aquifer <br /> SITE HISTORY <br /> In March 1991, three underground storage tanks (USTs) were removed from the site Analysis of { <br /> soil samples collected from the excavation indicated that high concentrations of petroleum <br /> hydrocarbons were present in soil beneath the tanks Groundwater was not encountered in the <br /> excavation The location of the former USTs is shown on Figure 2 <br /> In July 1993, a subsurface investigation was conducted at the site to determine the extent of <br /> petroleum hydrocarbons present in soil and to determine if groundwater had been impacted This <br /> included drilling eight soil borings and collecting soil samples Three of these borings were <br /> completed as shallow groundwater monitoring wells (MW-1, MW-2 and MW-3) Analysis of soil <br /> samples indicated that the majority of petroleum hydrocarbons in soil were present from about 10 <br /> feet below ground surface (bgs) to groundwater at a depth of approximately 29 feet bgs and <br /> within a radius of 35 feet from the former UST pit <br /> In August 1993, wells MW-1, MW-2, and MW-3 were monitored and sampled Analytical results <br /> showed that MW-1 had no measurable concentrations of petroleum hydrocarbons in the <br /> groundwater Wells MW-2 and MW-3 contained detectable levels of petroleum hydrocarbons A <br /> program of quarterly groundwater monitoring and sampling was begun in March 1994 <br /> w 1626051quaA1y0gr-1998 doc 1 <br />