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I <br /> system (VFS) was installed in August 1991 and was operated under permit requirements of <br /> the San Joaquin Air Pollution Control District order number 91-61 <br /> 2.3 Remediation of Hydrocarbon-Impacted Soil <br />' Remediation (soil vapor extraction) began to 1991, and progress has been summarized in <br /> reports submitted between March 1992 and February 1993 At the end of 1992, the VES had <br /> operated for approximately 8,884 hours, and the mean hydrocarbon vapor concentration at <br />' the inlet was approximately 500 ppm From the end of 1992 to July 1993, the VES was in <br /> operation for approximately 90 percent of the time, banging the total operational hours to <br /> 13,500. <br /> Hydrocarbon vapor concentrations ,%ere measured at the inlet to the VES, using a <br /> photoionization detector (PID), on a v eeKly basis to monitor the removal of hydrocarbons <br />' from the soil Vapor samples were collected on February 22 and April 28, 1993 for <br /> laboratory analysis The sample results were then correlated with the field readings This <br /> information was used to determine the volume and efficiency of hydrocarbon removal Sox] <br />' samples from borings CB-1 and CB-2, installed in June 1994, indicated the removal of 94C/c <br /> of petroleum hydrocarbons from the impacted soil The results of the samples "Here <br /> described in a Quaiterly Repoit dated July 17, 1993 <br /> 2.4 Regulatory Meeting <br /> On August 20, 1993, representatives of GeoAudit met Nvith 'N1r Ronald ]3r uno representing <br /> Genova Bakery, and Mrs Margaiet Lagorro of the PHS/El4D, to discuss further assessment <br /> and remediation activities A decision ,N as made to re-start the vapor extraction. motor and <br />' monitor vapor levels closely for several da)s to determine )vhetlrer additional benefit could <br /> be obtained by continuing to operate the system <br />' The combustion unit was re-started and operated from September 20 to September 26 and <br /> again from November 8 to December 7, 1993 The unit was shut-off on December 7, 1993 <br /> and has not operated since <br /> Using data obtained from the air samples collected dwrng the first half of 1993, actual <br />' concentrations of petroleum hydrocarbons were calculated to be 43% of the PID readings <br /> The last five PID readings ranged from 145 pprn to 242 ppm, this theoretically represents <br /> actual petroleum liydiocarbon concentrations of 62 ppm to 104 ppm The concentration of <br />' vapors removed frorn the soil at the site dulrng the re-start period (from September to <br /> November) was not significant It appeared that the continued operation of the vapor <br /> extraction unit would not significantly enhance soil mitigation at the site We recommended <br />' that the unit be permanently disconnected and vapor extraction at the site terminated <br /> cal,�i wasrv�. 1� 4 <br /> 0--B+Very QW112 NA 1 <br /> 1 <br />