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i <br /> i�TcAPPLIED TESTING CONSULTANTS <br /> MATERIALS ENGINEERING TESTING AND INSPECTION <br /> Nuclear Density Testing Report Per ASTM 1557 <br /> Report seq No <br /> cNerm Alliance Environmental Paye 1 of 2 <br /> ess 3060 Thomtree Drive,Suite 60 Date 6/4/98 <br /> City,state Chico, CA 95973 Tech M Haydon <br /> AM Willy Irwin <br /> Project Tank Removal Backfill, Stockton Aviation Airport Facility <br /> soil Description Tan Silty Sand <br /> Gauge a CALIBRATION DATA: Density Std std Dens4 xi xa <br /> �i Req'd% <br /> Equipment <br /> CLOW No T-1 Max Dry Density 108 3 opt Moist content 157 95% <br /> W Wet H2O Dry Moisture <br /> 7e � <br /> Test�! Te Location Eley DensityDensityDens Content Com Resuns <br /> 1 12' See Location Map FG-6' 1247 21 6 1032 209 96% PASS <br /> 2 12' See Location Map FG-6 1216 195 1021 191 95% PASS <br /> 3 12' Sea Location Map FG-4' 1218 198 1020 194 95% PASS <br /> 4 12' See Location Mae FG-9' 1 1255 202, 1053 1921 98% PASS <br /> 5 17 See Location Map FG-5 2' 1242 212 1031 20 5 96% PASS <br /> 6 12' ISea Location Map FG-3 5' 1217 174 1043 1671 97% PASS <br /> 7 12' See Location Map FG-4 5' 1 1201 1901 1011 188 94% OK <br /> 8 12" See Location Map FG-4' 121 5 185 10301 180 96% PASS <br /> 9 12' See Location Map FG-2' 1232 195 1037 188 96% PASS <br /> 10 12' 1 See Location Map FG-2' 12551 221, 1034 213 96% PASS <br /> REPORT <br /> Arrived at jobskte at 0700 hrs to perform compaction testing in backfill material placed in the tank removal <br /> area At the time of our arrival, the contractor had completed placing and compacting backfill material to an <br /> elevation of approximately 6 0' below Finish Grade(FG) An excavation was made to a depth of 9 0' below FG to <br /> check compaction in that portion of the backfill which had been completed prior to our arrival (Test No 4) <br /> Performed nuclear density testing from the 6 0'below FG elevation to the top of the backfill at random locations as <br /> material was placed Relative compaction test results along with coresponding elevations are indicated above For <br /> test locations, please refer to the attached location map Where test results indicated significantly less than the 95% <br /> relative compaction requirement, additional compactive efforts were applied until satisfactory compaction was <br /> achieved Based on the test results compiled on this project and witnessing the earthwork operations, it is our <br /> judgement that the backfill material placed in the excavation created by the tank removal was properly moisture <br /> conditioned and compacted to the requirements of the project plans and specifications and the applicable chapters <br />. of the 1994 UBC Departed jobsite at 1200 hrs <br /> CP+n to Rewerred by <br />