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iTcAPPLIED TESTING CONSULTANTS <br /> MATERIALS ENGINEERING TESTING AND INSPECTION <br /> Nuclear Density Testing Report Per ASTM 1557 <br /> Report 3" No <br /> cueat: Alliance Environmental Page 1 of 2 <br /> .ss 3060 Thorntree Dnve, Suite 60 Data 6/5x98 <br /> C4,5096 Chico, CA 95973 tech M Haydon <br /> Aft Willy Irwin <br /> project: Tank Removal Backfill, Stockton Aviation Airport Facility <br /> sou oewipum Tan Silty Sand <br /> Gauge a CABRATION DATA Dens ty Std std DensRy <br /> LIxi x, <br /> comP°uJOn Req'd% <br /> Equipment <br /> Curve No. T-1 I Max Ary Density 108 3 opt Moist content 157 95% <br /> Test Wet H2O Dry Moisture % <br /> Test a Depth Location Elev Density Density Densq Content Corno Results <br /> 18 12' See Locabon Map FG-1 0' 1210 180 1030 174 96% PASS <br /> 19 12' See Location Map FG-1 0' 121 8 188 1030 183 96% PASS <br /> 20 12" See Location Map FG 1192 179 1013 177 94% OK <br /> 21 12" See Location Map FG 1226 172 10541 163 98% PASS <br /> 22 17 See Location Map FG-1 0' 1231 210 1021 206 95% PASS <br /> 23 17 See Location Mae FG-1 0' 1200 179 1021 176 95% PASS <br /> 24 12' See Location Map FG 1209 181 1028 176 95% PASS <br /> 25 17 See Location Mae FG 1222 1921 1030 187 96% PASS <br /> 26 17 See Location Mae FG 121 6 193 102 4 188 95% PASS <br /> 27 12' See Location Map FG 12041 1821 102 2 178, 95% PASS <br /> REPORT <br /> Arrived at jobsite at 0800 hrs to perform compaction testing in backfill material placed around the tank <br /> removal area At the time of our arrival,the contractor had completed removing all clay soils beneath the future <br /> concrete slab to the satisfaction of the United States Army representative Backfill material was placed in V-8" <br /> loose lifts and thoroughly compacted with a vibratory smooth drum roller prior to placement of additional fill soils <br /> Nuclear density compaction tests were performed at randomly selected locations to verify that compaction <br /> requirements were being met Relative compaction test results along with corresponding elevations are indicated <br /> above For test locations, please refer to the attached location map Where test results indicated significantly less <br /> than the 95°x6 relative compaction requirement, additional compactive efforts were applied until satisfactory <br /> compaction was achieved Based on the test results compiled on this project and witnessing the earthwork <br /> operations, it is our judgement that the backfill material placed in the clay removal area beneath the proposed <br /> concrete drive slab was properly moisture conditioned and compacted to the requirements of the project plans and <br /> specifications and the applicable chapters of the 1994 UBC Departed jobsite at 1330 hrs <br /> Copies to <br /> Renewed by <br /> 3080 Thorntree Drive, Ste 35 • Chico, CA 95973 • Telephone (530) 891-6625 • Facsimile (530) 691-4243 <br />