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ARCHIVED REPORTS_XR0007692
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2900 - Site Mitigation Program
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PR0507153
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ARCHIVED REPORTS_XR0007692
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Entry Properties
Last modified
10/8/2020 10:41:12 PM
Creation date
6/23/2020 10:21:11 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0007692
RECORD_ID
PR0507153
PE
2950
FACILITY_ID
FA0007717
FACILITY_NAME
THRIFTY OIL #171
STREET_NUMBER
1250
Direction
N
STREET_NAME
WILSON
STREET_TYPE
WAY
City
STOCKTON
Zip
95205
APN
11731001
CURRENT_STATUS
02
SITE_LOCATION
1250 N WILSON WAY
QC Status
Approved
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LSauers
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EHD - Public
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GeoHydrologic Consultants, Inc <br /> . Table 7 2-3 Pumping Test Results for Drawdown TB-10 <br /> Aquifer Parameters Pumping <br /> ' Transmissivity(ft2/day) 1,150 <br /> ds= 0 07 <br /> Hydraulic Conductivity (ft/day) 2875 <br /> Storativity ----6-034 <br /> ' Groundwater Velocity (ftJday) 037 <br />' Stagnation Point (ft) 1635 <br /> 7.3 Groundwater Results <br />' The analytical results for the groundwater samples collected at beginning and at the end <br /> of the pump test from EW-5D are summarized in Table 9 Laboratory reports and chain- <br /> of-custody <br /> hain- <br /> ofcustody documentation are included in Appendix F <br />' The sample results indicated that moderate to high concentrations of TPHg and BTEX <br /> were detected Concentration for TPHg in groundwater at the beginning of the test was <br />' recorded to be 67,600 gg/L and at the end of the test it was 96,900 gg/L A similar <br /> increasing trend was observed for benzene (2,950 gg/L to 5,340 gg/L), toluene (8,250 <br /> gg/L to 16,200 gg/L), ethylbenzene (1,920 gg/L to 2,640 gg/L), and xylenes (11,200 <br />' <br /> µg/l_to 15,200 gg/L) MTBE on the other hand was not detected above the Iaboratory <br /> MDL of 0 18 gg/L in both samples <br /> 7.4 Pumping Well EW-5S <br /> Groundwater extract i on/mon iton ng well EW-5S is a 4-inch diameter well that is installed <br />' to a depth of 60 feet bgs, with 0 010-inch slotted well screen from 40-60 feet bgs The <br /> sand pack extends approximately two feet above the top of screen Groundwater appears <br /> to be present under unconfined water-table conditions Static groundwater was measured <br />' prior to conducting the pumping test in EW-5S at a depth of 47 05 feet bgs, indicating an <br /> estimated aquifer thickness of approximately 40 feet <br />' The pumping test was started at 6 50 AM on April 6, 2005 and was maintained at a <br /> constant pumping rate of approximately 0 25 gallons per minute (gpm) for 730 minutes, <br /> terminating at 7 00 PM that evening, with a maximum drawdown of 5 80 feet in EW-5S <br />' at the end of the test A total of approximately 135 gallons of water was removed during <br /> the pumping test and stored onsite in a 4,000-gallon polyethylene Baker Tank All water <br /> . generated during the test was vacuum trucked from the tank and properly <br /> I <br /> TQC 171 Pdot Study Page 21 <br />
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