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ARCHIVED REPORTS_1995_1
EnvironmentalHealth
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4400 - Solid Waste Program
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ARCHIVED REPORTS_1995_1
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Last modified
7/17/2020 6:26:40 PM
Creation date
7/3/2020 10:41:08 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
4400 - Solid Waste Program
File Section
ARCHIVED REPORTS
FileName_PostFix
1995_1
RECORD_ID
PR0440004
PE
4433
FACILITY_ID
FA0004517
FACILITY_NAME
FOOTHILL LANDFILL
STREET_NUMBER
6484
Direction
N
STREET_NAME
WAVERLY
STREET_TYPE
RD
City
LINDEN
Zip
95236
APN
09344002
CURRENT_STATUS
01
SITE_LOCATION
6484 N WAVERLY RD
P_LOCATION
99
P_DISTRICT
004
QC Status
Approved
Scanner
SJGOV\rtan
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FilePath
\MIGRATIONS\SW\SW_4433_PR0440004_6484 N WAVERLY_1995_1.tif
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EHD - Public
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KLEINEELDER <br /> File No. 24-2206-O1.A06 <br /> January 2, 1991 <br /> Y <br /> been classified according to the Unified Soil Classification <br /> System, described on Plate A-2 . <br /> LABORATORY TESTS <br /> Laboratory tests were performed on a variety of samples obtained <br /> from the ex-oloratory borings in order to evaluate permeability and <br /> gradation characteristics of the soils encountered. The tests <br /> consisted of Hvdrometar and Falling Head P2=meabil4ty. The results <br /> of our Hydrometer tests are noted on the Summary of Laboratory <br /> Tests, Platz A-13 . <br /> CONCLUSIONS AND RECOMMMMAMATIONS <br /> Phase I Area Sails for Clav Liner <br /> For this study our firm performed a total of 13 Falling Head <br /> Permeability tests on various samples, mostly in their in-situ. <br /> state. The tests were performed in accordance with The Corps of <br /> Engineering manual, Test ,SEM 110-2-1906, with an effective <br /> confining pressure of 4 pounds per sctuare inch. In addition, a <br /> total of 5 tests were performed for our earlier 1985 study. The <br /> results of our Falling Head Permeability tests are as follows: <br /> October 1990 <br /> Coefficient <br /> Boring Depth of Permeability <br /> Sample (ft) Description k, (cm/sec) Moisture % ncf <br /> B-1 20 Silty Clay 7. 4 x 10-5 79 37 <br /> B-1 3 Cemented <br /> Sandy Silt 2 . 8 x 10-4 87 21 <br /> B-2 5 Silty Clay 2 .8 X 10-4 58 40 <br /> B-2 30 Cemented <br /> Sandy Silt 1. 4 X 10-3 86 16 <br /> Copyright 1991 KLeinfeider, Inc. 4 <br />
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